8 January 1964 | F-104G | MM6509 / 4-9 | 4St/9gr | AMI | written off | pilot killed |
10 January 1964 | CF-104 | 12767 | 6STR-OTU | RCAF | written off | pilot ok |
10 January 1964 | CF-104 | 12779 | 6STR-OTU | RCAF | incident | pilot ok |
15 January 1964 | CF-104 | 12828 | 422sq | RCAF | incident | pilot ok |
This Starfighter encountered an electrical failure during a standard mission while crossing Ramstein area. The pilot performed a successful emergency landing and the aircraft was repaired soon. |
16 January 1964 | F-104A | 56-830 | 319FiS | USAF | written off | pilot ok |
This accident occurred after the aircraft departed Homestead AFB, Florida and flying a low-altitude intercept mission. It flew as wing man, 2,500 to 3,000 feet. 20 minutes after take-off and 5 minutes after the practice intercept at approximately altitude of 10,000 feet, when the pilot heard a bang of moderate loudness and a continuing roar. Engine RPM seemed to be decreasing. Pilot assumed he had a flame-out or compressor stall and stop-cocked the throttle and activated both start switches. RPM decreased to 45% and EGT steadily rose. Three additional start attempts were made with similar results. Generators went off line at approx 65% RPM and electrical power was lost. With engine RPM at 25% the pilot, Captain James "Jim" Milner, decided to eject. Ejection was safe and the pilot landed in open water and climbed into his life raft. He was rescued after approx 80 minutes. Location of the crash appears was 65 nautical miles NE of Homestead AFB. The aircraft was not recovered. Investigation showed that the engine failure was caused due to cracks in the nozzle diaphragm (turbine stator assembly just forward of the first stage turbine). The stator blades bent back into the first stage turbine causing compressor stall from which there was no recovery. The whole Starfighter fleet was inspected afterwards. The IFS owns a copy of the official USAF accident report. |
16 January 1964 | TF-104G | D-5807 | TDM | KLu | incident | pilot ok |
17 January 1964 | CF-104 | 12854 | 1W | RCAF | incident | pilot ok |
During a mission over Marville area this CF-104 encountered a small explosion inside its engine. Gladly the aircraft could land safely and returned back to operational service soon after. |
20 January 1964 | CF-104 | 12870 | 444sq | RCAF | incident | pilot ok |
During a standard flight this Starfighter encountered loss of power on a certain moment. Gladly a restart was possible and it could make a successful emergency landing. |
22 January 1964 | F-104B | 57-1306 | 319FiS | USAF | written off | pilot ok |
27 January 1964 | CF-104 | 12858 | 430sq | RCAF | written off | pilot ok |
This Grostenquin based Starfighter crashed after an engine-failure at low level near Metz, France. The pilot, FlLt. Van Vliet ejected safely. The cause was a nozzle closure problem. The report stated that it when on a routine training mission, the pilot realized that the afterburner nozzle had malfunctioned, remaining in an open position. After attempting an emergency closing (ENCS) which failed, the pilot set up a course for return to base above a low under cast. Following ENCS attempt, the nozzle went to full wide open and the oil low level light flashed on. A burner climb to 32,000 feet was followed by a glide toward base. During a second burner climb the pilot had an extended conversation with two other pilots and several persons on the ground. The pilot’s problem was whether to descend through the under cast and attempt a failed nozzle landing in weather of 2500 and 2½ with the possibility of oil starvation and engine seizure. The pilot elected not to attempt a landing. The ejection at 12,000 feet was successful. |
31 January 1964 | F-104G | 7091/VA+111 | MFG1 | GNavy | written off | pilot ok |
31 January 1964 | F-104G | 7092/VA+112 | MFG1 | GNavy | written off | pilot ok |
18 February 1964 | F-104B | 57-1308 | AFSC | USAF | written off | pilots ok |
3 March 1964 | F-104D | 57-1329 | 476TFS | USAF | written off | pilots ok |
This Europe deployed Starfighter crashed in Spain while based at Moron AFB following an in-flight fire as a result of inflight refueling. Both crew, Major James J. Thomas and Captain Robert J. Lenar (flight surgeon),ejected safely with no injuries. It was on a day-night refueling mission on KC-135 with a scheduled 4 hook-ups for each pilot and included a short cross-country and instrument letdowns and GCI intercepts in between refuels in a flight of three. The flight also consisted of No. 2 Lt. Beall in F-104C 56-919 and No. 3 Lt. Vivian in F-104C 57-915. The F-104D 57-1329 was flight leader and configured with tip tank; both F-104Cs in the flight were clean. The second tanker rendezvous was made at 1858 (20 minutes before official sunset). After being hooked up for approximately one minute, Lt Thomas in 57-1329 felt a mild thump. A check of the aircraft and instruments revealed nothing but 15-to-30 seconds later the tanker boom operator noticed the tip tanks siphoning fuel. 57-1329 then backed off the drogue after receiving 2,800 lbs. At the time the refueling boom disconnected from the drogue both occupants of 57-1329 felt the same intensity of thump. The boom operator noticed a flash. Major Thomas then noted a warning lightin the gear handle and reduced power and he recycled the gear. He then transmitted that he had a hung gear door and at 230 knots he recycled the gear again to re-engage the door up lock hooks. Lt. Vivian in No. 3 noted the right main gear door in the down position and the tips siphoning fuel. All aircraft were leaving contrails and it was difficult to distinguish a fuel overflow from a contrail. Then Lt Vivian in No. 3 saw a ball of fire erupt from the vicinity of the wheel well of 57-1329. A transmission was made to Major Thomas that he was on fire but then he was told the fire ball disappeared. 57-1329 was slowing down rapidly and Lt Beall and Lt Vivian could not pace him even with idle power, speed brakes out and maneuvering flaps down. As 57-1329 re-advanced the throttle the “SLOW” light started blinking on. Engine RPM remained at 70% and he noted EGT at 580 degrees C. Also, a series of thumps continued. Major Thomas believed he had a compressor stall and initiated stall clearing procedure. He stop cocked the throttle, hit the air start switches, and re-advanced the throttle to Military. RPM stayed at 70% EGT fuel flow (nozzle positions were not noted). Lt Vivian noticed balls of fire erupting from the underside of 57-1329 at about the gear well. Lt Vivian radioed Major Thomas that he was on fire and to bail out immediately. At this same time fire warning lights came on in 57-1329. The UHF radio went dead. No other lights were noted. The intensity of the fire increased and flames were trailing from the aircraft for 200 feet with the underside glowing red. Major Thomas ordered Capt Lenar to bail, and when he had safely ejected Major Thomas left the aircraft. The entire sequence of events from disconnect from the drogue to the bailout was one minute and eight seconds.After the pilots ejected, the aircraft rolled into a steep spiral and was seen to impact on the ground in a near vertical dive, approximately 58 nautical miles and 96 degrees magnetic from Moron Air Base, Spain.. Captain Lenar landed safely in an open pasture. Major Thomas came down in a small olive tree which cushioned his landing. They were returned to base some hours later by the car which was sent to pick them up. The F-104D crashed. The accident was caused by an over pressurization of the internal fuel cell bladder of the D which caused a fuel leak in the left intake near the generators, The leaking fuel was leaking through the inside aluminum panel, and was mixing in with the intake air and was being ignited by the generator. Eventually the aircraft caught on fire. The International F-104 Society owns a copy of the official accident report. |
5 March 1964 | CF-104 | 12752 | 6STR-OTU | RCAF | written off | pilot ok |
17 March 1964 | QF-104A | 56-746 | 3205DS | USAF | written off | no pilot |
This day was the first time in 1964 that the Eglin based drone squadron lost again one of its drone Starfighters. The QF-104A was completely destroyed after it was successful shot down by a BOMARC missile. |
17 March 1964 | TF-104G | MM54226 | Lockheed | AMI | incident | pilots ok |
24 March 1964 | F-104G | 2071/DC+101 | JBG33 | GAF | written off | pilot ok |
24 March 1964 | F-104D | 57-1324 | 435TFS | USAF | incident | pilots ok |
1 April 1964 | F-104A | 4202 | 8TFS | RoCAF | written off | pilot ok |
22 April 1964 | F-104G | 2049/DA+232 | JBG31 | GAF | incident | pilot ok |
1 May 1964 | CF-104 | 12809 | 3W | RCAF | written off | pilot ok |
This aircraft crashed after a nozzle-failure on GCA-approach to home base Zweibrucken. The pilot, FlLt. D.E.Wilson ejected safely. It all happened when the pilot was flying downwind on GCA at 3th Wing when his oil low level light came on momentarily. He broke off the GCA and headed for base, however, after selection of Land Flap, the light reappeared and the nozzles opened fully. The pilot actuated his afterburner immediately and made an overshoot and climbed back to the circuit but suddenly the afterburner failed and was not able to relight.. The Emergency Nozzle Closure System was activated but failed, the nozzle stayed open.. After a while when the altitude and speed were below safe conditions the pilot ejected. He landed between some trees 1.5 miles away from the point of impact of his aircraft and did not sustain any injuries gladly. |
2 May 1964 | F-104G | 8018/JA+106 | JG71 | GAF | written off | pilot killed |
This Starfighter crashed near Bremerhafen after touching the ground during a flying demonstration. The pilot, USAF Major Thomas E. Perfili (37) was killed instantly. |
8 May 1964 | TF-104G | 62-12272 | 335Mira | HAF | written off | pilots killed |
11 May 1964 | F-104F | BB+381 | WS10 | GAF | incident | pilots ok |
11 May 1964 | RF-104G | 8142/EA+233 | AKG51 | GAF | written off | pilot ok |
This Starfighter crashed near Manching after an engine failure. Hptm Norbert Senger ejected safely. Aircraft was completely destroyed. |
11 May 1964 | F-104G | 8036/JA+232 | JG71 | GAF | written off | pilot killed |
11 May 1964 | CF-104 | 12811 | 3W | RCAF | written off | pilot ok |
This aircraft crashed after a disconnect of the rudder linkage during flight near Zweibrucken. The pilot, FlLt. L. S. Bentham ejected safely. The aircraft was on a low-level exercise when it suddenly yawed violently. The pilot immediately pulled up, switched off the yaw damper and tried the trim control but the yaw remained. By looking through the rear-view mirror he could see that the rudder was deflected fully to the left. He then went through all the prescribed procedures but to no avail, the rudder remained fully left, the ball fully right and although the rudder pedals would move, they had no effect whatsoever. The pilot declared an emergency, headed for base and requested technical advice from the tower. Finally, after about 40 minutes, a technical adviser arrived in the tower but he was able only to suggest procedures that had already been tried by the pilot. As it turned out, the long delay was of no consequence, the pilot could have done nothing to correct the rudder malfunction. The pilot was faced with a critical decision; attempt a landing or bail out. He found that he could retain control down to 190 kts but at this speed about 15 degrees of bank was required to hold its heading. An approach was attempted at home base where there was 90 degree crosswind. Just before touchdown at about 50 feet he found that excessive bank was required to keep on runway heading and had to overshoot. The pilot diverted to a nearby USAF base with a runway into the wind. However, when he picked up the runway visually at 1½ miles, a 150 degree turn would have been required to lineup. By this time fuel was down to 400 lbs and the area heavily populated. The pilot decided another approach under these circumstances would be unwise. He proceeded to the bail out area and with a fuel state of zero, ejected. Everything worked as advertised and the pilot landed in trees with only a few minor scratches and bruises. The aircraft crashed in open country and caused no damage. Inspection of the wreckage revealed that a cotter pin had not been installed (probably during manufacture) in a bolt in the rudder assembly. However, the missing cotter pin had escaped detection on two periodic inspections. The bolt had worked free and a spring had pushed the rudder to full left deflection. |
14 May 1964 | F-104A | 56-829 | 319FiS | USAF | incident | no pilot |
This Starfighter was slightly damaged at McClellan Air Force Base due to an non-flying incident on the ground. The damage could be fixed soon and it was flown back to 319FIS at Homestead Air Base on May 18th. |
28 May 1964 | F-104D | 57-1325 | 479OMS | USAF | written off | pilot ok |
May 1964 | F-104G | 237/FN-A | 331Skv | RNorAF | incident | pilot ok |
(USAF 62-12237) During a visit of some Norwegian Air Force F-104s to Bentwaters in the UK, from 6 till 13 May 1964, this aircraft encountered an incident. It had to abort the take off due to stuck controls. The pilot selected its arresting hook and caught successfully the arresting wire at the end of the runway. The aircraft could be repaired at Bentwaters before its intended departure on May 13th. |
4 June 1964 | F-104G | FX-06 | 1W | BAF | incident | pilot ok |
This Starfighter ran off the runway during difficult weather conditions. A combination of a heavy landing and wheel shimmy resulted in loss of control. Pilot Capt B. Bastiaens was ok and the aircraft could fly again soon. |
15 June 1964 | F-104A | 56-764 | AFFTC | USAF | written off | pilot ok |
25 June 1964 | CF-104 | 12778 | 6STR-OTU | RCAF | written off | pilot ok |
This Starfighter crashed after a compressor-stall on low level flight near Cold Lake. The pilot, FlLt. W.G.Baker ejected safely. No specific evidence of bird strike in spite of assumption. A T-33 went out for searching the aircraft crash location. |
26 June 1964 | CF-104 | 12823 | 427sq | RCAF | incident | pilot ok |
Lt. N.A. MacSween landed his aircraft at home base Zweibrucken at a near full fuel load just after takeoff after he detected smoke in the cockpit. The pilot took the barrier and subsequent investigation proved the radar electronics to have caught fire. The aircraft could be repaired again. |
2 July 1964 | F-104G | 7102/VA+122 | MFG1 | GNavy | incident | pilot ok |
This day this Navy Starfighter made a crash landing at home base Jagel where it run off the runway. The pilot was fine and the aircraft could be repaired. |
10 July 1964 | JF-104B | 57-1301 | AFSC | USAF | incident | pilots ok |
This modified test Starfighter suffered an accident at Eglin Air Force Base during the landing. It happened at 13:35 CST. The aircraft belonged to the 3214th OMS located at the Air Proving Ground Center at Eglin Air Force Base. Coming back from a 1 hour uneventful training flight to their home base they requested an overhead pattern followed by a full stop. On base they reported “Three wheels”. The aircraft touched down slightly over 1,000 ft down the runway. At 1,400 ft the right tip tank fin struck the ground the first time. The tip tank scraped the runway several times until the aircraft departed the runway 2,300 ft from the approach end. Leaving the runway the pilot in the front ejected followed by the rear seat pilot. Both ejections were sadly fatal due to too low altitude. Shortly thereafter the aircraft came to a stop. The aircraft could be repaired again. It is strange that Capt. Richard E. Hockenberry and 1lt. Robert W. Sullivan both ejected while they were too low. Both sadly died due to the injuries. The International F-104 Society owns a copy of the official accident report. |
23 July 1964 | F-104G | MM6596/5-21 | 102gr | AMI | written off | pilot killed |
27 July 1964 | F-104F | BB+380 | WS10 | GAF | written off | pilots ok |
7 August 1964 | CF-104 | 12844 | 422sq | RCAF | written off | pilot killed |
This Starfighter struck a hill and exploded near Dijon, France in bad weather conditions while flying low-level mission. Pilot, FlLt. I.W. MacLean did not eject and was sadly killed. |
18 August 1964 | F-104G | FX66 | SABCA | BAF | written off | pilot killed |
3 September 1964 | F-104A | 56-803 | 9sq | PAK | written off | pilot killed |
This Starfighter crashed during a low pull-out, F/L Tariq Majeed was sadly killed. Photo beneath, showing this unlucky aircraft, was achieved thanks to the Pakistan Air Force. |
11 September 1964 | F-104G | MM6555/21-14 | 21gr | AMI | written off | pilot killed |
9 October 1964 | F-104J | 46-8583 | 202sq | JASDF | written off | pilot ok |
This Japanese F-104J Eiko crashed into the sea 10km South South East of home base Nyutabaru due to flap-malfunctioning while performing an air to air firing training mission. It happened at 2:50PM. The pilot 2nd Lt. Kuroki Norihisa ejected safely. The aircraft was third of a flight of 4 aircraft which flew towards the sea near Hyuuga. Suddenly flaps and radio malfunctioned. Pilot signaled his other formation pilots using his hands and headed back to base accompanied by his wing man. While returning to base, the pilots was not able to solve the malfunction. Approaching the base, the air base command declared a landing without flaps would be too difficult, and at 14:45 the air base command authorized the wing man to order the pilot to ditch his aircraft by guiding him to the sea. At 14:50, aircraft flew above sea, and pilot ejected and was soon recovered by a rescue helicopter. The aircraft crashed into the sea about 5 km South East of Ichinose River mouth. |
10 October 1964 | F-104A | 4205 | 8TFS | RoCAF | written off | pilot killed |
10 October 1964 | F-104A | 4212 | 8TFS | RoCAF | incident | pilot ok |
10 October 1964 | F-104A | 4216 | 8TFS | RoCAF | written off | pilot killed |
14 October 1964 | F-104G | 7136/DD+237 | JBG34 | GAF | written off | pilot killed |
This Starfighter crashed near Unterschwartzach and Memmingen, Germany. The cause of the accident was spatial disorientation. Sadly Hptm. Gunther Klatt was killed. |
16 October 1964 | F-104C | 56-927 | 476TFS | USAF | written off | pilot ok |
16 October 1964 | F-104G | 2085/DC+236 | JBG33 | GAF | written off | pilot ok |
19 October 1964 | F-104G | 7065/DC+250 | JBG33 | GAF | incident | pilot ok |
27 October 1964 | CF-104 | 12849 | 439sq | RCAF | written off | pilot ok |
29 October 1964 | F-104G | MM6597/5-22 | 102gr | AMI | written off | pilot ok |
This AMI Starfighter crashed near its home base Rimini when the pilot, Ten. Mario Giammona, experienced a APC (Automatic Pitch Control) intervention after a low pass over the airbase. Because the aircraft was too low to recover normally the pilot ejected and was safe although he got injured. |
10 November 1964 | F-104A | 56-860 | 319FiS | USAF | written off | pilot ok |
12 November 1964 | RF-104G | 8126/EA+115 | AKG51 | GAF | written off | pilot ok |
This reconnaissance Starfighter crashed near home base Manching after Major Charles Learnard (USAF) experienced an engine failure and had to eject. He was safe. |
16 November 1964 | CF-104 | 12856 | 3W | RCAF | written off | pilot ok |
17 November 1964 | F-104G | D-8045 | 322sq | KLu | written off | pilot killed |
This Starfighter crashed, after it run out of fuel, into the mountains near Trondheim, Norway some 25 km south-east of Kristiansund, near Straumsnes, Tingvoll. The pilot (322 squadron commander) Major Willem "Bill" Heitmeijer (39) was sadly killed. The cause was oxygen-mask poisoning which made the pilot unconscious. In the morning (09:21 zulu time) Major Bill Heitmeijer toke off (Mission 07) from Leeuwarden Air Base, together with Lt. Eric Dames, to the south for a navigation trip. Around 09:38 Z both returned back heading Leeuwarden. Reaching the Friesland county at approx. 30.000 ft, being on autopilot, something was wrong with Major Bill Heitmeijer. All radio contact was lost with him and the aircraft flew on heading the North-North-East in a straight line. Immediately wing man Lt. Dames attempted to awaken the pilot but after a while when he ran out of fuel he had to go back to Leeuwarden around 10:10 Z with only 1000 lbs fuel left. Around 12:00h local time his attempts were taken over by a Norwegian Air Force F-86 Sabre which had taken off from Rygge Air base around 10:45 Z. The F-86F pilot, Lt Col Arne Riegels, arrived with the D-8045 at 11:00 Z and flew very close to the Starfighter. He checked the pilot but the pilot was unconscious or maybe dead. He even brought the F-104 inside the jet-wash of his F-86 but also these tabulations did not have any effect any more. Suddenly the Starfighter dived vertical from 200 meter and finally crashed into the mountains. This was the moment that the aircraft ran out of fuel. Time was 11:17 Z, almost 2 hours after the Starfighter took off from Leeuwarden AB. As already mentioned, the official investigation showed that the accident was caused by oxygen mask poisoning, a reason to initiate a special treatment of oxygen mask cleaning and checking within the NATO Air Forces. Only half of the engine could be covered and the rest of the aircraft disintegrated. Currently still a lot of debris including a big part of the J-79 engine can be found at the memorial location. This location can be found at coordination N 62 59, 495 - E 008 03,161 and is just beneath the mountain Nipa, in Tingvoll Borough. The plate on the memorial shows a number of interesting radio conversation during the tragic ending mission. Beneath some photos of the aircraft, the memorial which includes parts of the aircraft, a map with given route and two newspaper articles regarding the accident. Thanks to Peter Rhebergen and Geir Lorentzen. See also: https://docplayer.me/106717409-1964-en-ukjent-grav-pa-vaernes.html. |
@ |
##
Back to accidents overview |
Copyright © 2024 I-F-S.NL Protected by U.S. and International law for the F-104 Society Inc. The Netherlands | Developed by Media4ever and Ralphdesign