8 January 1963 | JF-104B | 56-3720 | AFSC | USAF | written off | pilots ok |
10 January 1963 | F-104A | 56-829 | 157FIS | SC ANG | incident | pilot ok |
6 February 1963 | QF-104A | 56-734 | 3205DS | USAF | incident | no pilot |
This QF-104A "QFG-734" engaged the barrier on landing like it did as well in 1962. The aircraft did not brake and did not release its drag chute. This could have been the result of a failure of "weight on nose gear switch" malfunction. The aircraft could soon continue with the drone operations. |
6 February 1963 | F-104C | 56-899 | 436TFS | USAF | written off | pilot ok |
18 February 1963 | CF-104 | 12777 | 6STR-OCU | RCAF | written off | pilot killed |
19 February 1963 | F-104D | 57-1321 | 4443CCTS | USAF | incident | no pilot |
15 March 1963 | F-104C | 57-922 | 435TFS | USAF | incident | pilot ok |
This F-104C landed at the the runway with its gear up at Edwards AFB. The pilot, Captain Charles E. Connors with 479-TFW, 435-TFS, was not injured. Following a successful BDU-8 practice bomb dropping mission out of George AFB Captain Connors and Captain Harvey Quakenbush joined up when Capt Connors noted a slight loss of thrust and his Lead (Capt Quackenbush) observed that he was siphoning. Capt Connors then noted that his nozzles were open and selected AB and obtained AB light. A climb was initiated to 31,000’ over Edwards AFB Runway 22. The AB was shut down and emergency nozzle closure handle was pulled. This action did not close the nozzles. A precautionary pattern was entered with the throttle in idle, speed brakes in, gear up, and flaps in t/o position. The aircraft was flown to final approach with no difficulty with the airspeed at 295 knots. At this time Capt Connors put out the speed brakes to slow down. The gear was put down at 265 knots approximately over the approach end of the runway at Edwards AFB. The pilot felt he was getting no indication of the gear coming down so he placed the landing lever in the Up position and inadvertently pulled the drag chute handle instead of the manual landing gear release handle. Capt Connors realized he had pulled the wrong handle and immediately placed the landing gear lever to the Down position again. Shortly after the drag chute deployed the aircraft contacted the runway with the landing gear in the Up position. Final fix: A possible fix on reliability of main fuel control was the installation of Project "Hard Core" main fuel filters on the -3B engine. The IFS owns a copy of the official USAF accident report. |
10 April 1963 | F-104J | 26-8504 | 2W-201sq | JASDF | written off | pilot killed |
12 April 1963 | F-104C | 56-896 | 435TFS | USAF | written off | pilot ok |
This Starfighter crashed North of interstate 15 (I15) at Soda Mountains near the town of Baker, California, pilot Keith Davey ejected safely, The pilot stated : "We briefed a two ship flight, myself and Richard Lougee of the 435th TFS. Dick was lead and I flew wing on a low level to Cuddeback Range. I don't recall what the range mission was but we carried an MN-1A dispenser with 25lb. practice bombs as well as tip tanks. After takeoff we flew in spread formation proceeding towards Baker, CA. Crossing a dry lake I noted a slight bump and shortly thereafter the control stick began to stiffen, requiring abnormally high force to move it. A check of the hydraulic pressures revealed a problem, the guages were oscillating rapidly, down toward the bottom of the scale. The control stick froze and control with it was pretty well lost at this point. I found by going into burner I could raise the nose and could keep wings level or turn with the rudder, which was manual on the "C". The ailerons began "flopping in the breeze" and the whole airframe was unstable, however I could control if fairly well at this point, and attempted to head towards Edwards AFB, as we always did with a problem, hoping to get it down on the long runway or lake bed there. As control deteriorated, I deployed the RAT but it didn't seem to have any effect. I was able to fly level at about 10,000 feet for a short time but the stab evidently shifted and I couldn't keep the nose up. As airspeed increased past 400kts and the nose continued to drop, I had no choice but to eject. I told Dick of my plan, blew the canopy, and pulled the ring". Keith landed succesful with his chute in a rocky environment and soon after an H-13 helicopter arrived. This helicopter damaged its rotor on landing and so another helicopter was arranged, a Navy H-34 from Cold Lake. Both Keith and the other helicopter pilot were dropped at Fort Irwin. An Air Force Helicopter from George AFB took Keith back home. The IFS owns a copy of the official USAF accident report. |
24 April 1963 | F-104C | 57-918 | 436TFS | USAF | written off | pilot killed |
30 April 1963 | JF-104C | 56-888 | AFSC | USAF | written off | pilot ok |
10 May 1963 | F-104C | 57-912 | 435TFS | USAF | written off | pilot ok |
27 May 1963 | CF-104 | 12719 | 4W | RCAF | written off | pilot ok |
This Baden-Sollingen based Starfighter crashed after an engine flame-out on an initial acceptance flight, near Colmar. The pilot, FLt L.A. Tapp ejected safely |
6 June 1963 | QF-104A | 56-730 | 3205DS | USAF | incident | no pilot |
18 June 1963 | QF-104A | 56-730 | 3205DS | USAF | written off | no pilot |
19 June 1963 | CF-104 | 12728 | 6STR-OCU | RCAF | written off | pilot killed |
This Cold-Lake based aircraft struck ground after take-off, probably caused by an open canopy. The pilot, FlLt. W.G.Hollingshead used his ejection-seat at too low altitude and was killed. The aircraft crashed near Cold Lake. |
16 July 1963 | F-104G | FX08 | 1W | BAF | written off | pilot ok |
This Starfighter crashed near Taviers after pilot, kapt. Georges Castermans encountered a fire-alarm. The pilot was ordered to eject which was sucessful. It was the first Belgium F-104 loss. The pilot stated: After experiencing a BLC duct failure on final approach to Beauvechain (with 50 hours experience on F-104-F/G). A split second reaction to revert to T/O flaps saved my life but the fire warning lights, an unexpected T2 reset and other problems forced me to abandon the A/C. The FX08 flew an ordinary training flight with another F-104 practicing PI's (Practice interceptions) and returning to base for GCI/GCA landing. Investigation found out that the same hot air was sucked forward to the engine front where the CIT sensor (Compressor Inlet Temperature) was positionned at 6 o'clock which registered an abnormally high temperature which caused a T2 reset (acceleration of RPM to 102 % whatever the position of the throttle) only occuring normally at high altitude when nearing Mach 2, to avoid a compressor stall. The air coming out of the 13th stage of the compressor at full RPM was at 650° C. |
23 July 1963 | CF-104 | 12802 | 427sq | RCAF | written off | pilot killed |
24 July 1963 | CF-104 | 12816 | 434sq | RCAF | written off | no pilot |
25 July 1963 | F-104A | 56-814 | 319FIS | USAF | written off | pilot killed |
1 August 1963 | QF-104A | 56-734 | 3205DS | USAF | written off | no pilot |
This day this QF-104A "QFG-734" was shot down as unmanned drone by a BOMARC missile during live shooting exercises. Aircraft remains crashed into the sea. |
![]() |
1 August 1963 | QF-104A | 56-735 | 3205DS | USAF | incident | no pilot |
8 August 1963 | F-104G | KG+180 | Fokker | GAF | incident | pilot ok |
21 August 1963 | F-104C | 56-933 | 479TFW | USAF | incident | pilot ok |
This aircraft suffered damage to the horizontal stabilizer when the front fairing of the left AIM-9B launcher departed in flight over Death Valley, California. The pilot, Captain Charles E. Connors with 479-TFW, 479-OMS, landed without incident. The flight was briefed for an air combat tactics mission with captive AIM-9B (GAR-8) missiles installed. Capt Connors was to fly wing position during the flight. All phases of flight proceeded normally and as briefed until joinup for return to the field. At this time the lead pilot noticed the front fairing of the left AIM-9B launcher was missing. No further damage was noted at this time and the flight was terminated without further incident. The damage to the horizontal stabilizer was discovered while the aircraft was shutting down in the refuelling area. Location : California, Inyo, Death Valley, 50NM radius of Furnace Creek. TAC 12thAF, 831st AD, 479TFS, 479OMS, George Air Force Base. The IFS owns a copy of the official USAF accident report. |
28 August 1963 | F-104B | 56-3721 | AFFTC | USAF | written off | pilots ok |
5 September 1963 | RF-104G | D-8050 | 306sq | KLu | written off | pilot killed |
11 September 1963 | CF-104 | 12794 | 427sq | RCAF | written off | pilot killed |
27 September 1963 | TF-104G | D-5802 | TDM | KLu | incident | pilot ok |
This day this Starfighter encountered a bird strike during its the landing at homebase Twenthe AB. It could land but sustained damage which needed to be repaired. |
3 October 1963 | QF-104A | 56-836 | 3205DS | USAF | written off | no pilot |
The QF-104A QFG-836 was shot down as unmanned drone by a GAR-2B missile from another fighter, during live shooting exercises. The aircraft was completely destroyed and crashed into the sea. |
8 October 1963 | QF-104A | 56-739 | 3205DS | USAF | written off | no pilot |
10 October 1963 | F-104G | DC+102 | JBG33 | GAF | incident | pilot ok |
22 October 1963 | CF-104 | 12876 | 444sq | RCAF | written off | pilot ok |
24 October 1963 | CF-104 | 12793 | 427sq | RCAF | written off | pilot killed |
30 October 1963 | F-104G | 61-2603 | 4443CCTS | USAF | written off | pilot ok |
It crashed while being used at George AFB for training (NATO/MAP). Royal Netherlands Air Force Major Henricus W. Arendsen was flying this Starfighter Transition Mission #8. This is the second solo F-104G mission of the course. The training syllabus does not require a chase pilot for this mission but local policy provides for an observer pilot. Weather in the flying area at the time of the accident was clear, visibility 10 Miles, wind WNW at 18knots. The flight was thoroughly planned by Captain John P. Gee, the observer instructor pilot. Major Morton C Mumma, III, USAF student instructor pilot flew Captain Gee's wing. Major Arendsen was the number 1 aircraft of the three. He was briefed to line up on the runway, perform his pre-takeoff checks and takeoff as a single aircraft. Immediately after takeoff Major Arendsen noted an unsafe gear indication. This difficulty was remedied by recycling the gear. (Any delay on gear retraction on takeoff usually results in the gear doors not locking closed due to the rapid build up of air loads associated with the very raped acceleration of the aircraft. Although briefed on this possibility, students in the transition phase experience this condition occasionally. Captain Gee and Major Mumma took off as an element and flew as observers for Major Arendsen in the local transition area. While proceeding to the local transition area Major Mumma flew in trail on Captain Gee to gain experience with the F-104G radar. At 22.000 feet and in the local transition area Major Arendsen performed steep turns and other aerobatic maneuvers which included loops, barrel rolls and lazy eights. While doing the previous mentioned maneuvers some altitude was lost and climb was made with afterburner in an attempt to position the aircraft for another loop. At this time he arrived at an altitude of approximately 23,000 feet, 160 knots, on a heading of about 330 degrees. From this point a diving turn was initiated to the right in an attempt to set up the conditions for another loop.Major Arendsen established a 60-70 degree dive angle at this time. The aircraft configuration was takeoff flaps down and the throttle at full military. During the course of the dive, although the pilot could not recall the sequence, he applied back pressure to the stick, retracted the takeoff flaps and experienced kicker three times. Between the second and third kicker he extended the speed brakes and retarded the throttle to IDLE and after the third kicker he ejected. Although the pilot has no recollection of the altitude at which he ejected, for the available evidence it is estimated that ejection occurred at between 2000 and 5000 feet above the terrain. The aircraft struck the ground at the estimated dive angle of 50 to 80 degrees and exploded on impact. The pilot sustained two broken legs. Major Mumma and Captain Gee remained in the vicinity of the crash long enough to alert a rescue helicopter from Fort Irwin. They then returned to George Air Force Base and landed. Lateron Major Arendsen revealed: "After I had done some aerobatics. I set myself up for a loop and then I realized that I wasn't on the flatter part of the country but that I was over the hills. Then I saw that I couldn't make the pull out and got the kicker three times. After the third time I decided to bail out." Investigation: The aircraft hit the ground on the easterly heading at a steep dive angle. Most of the wreckage was found within a 1000 foot area east of the impact area. The wing flap actuators showed the flaps had been in the UP position. The tachometer showed the RPM to be 70% (IDLE). There was no evidence to indicate flight control positions at impact. Since the pilot testified that he was satisfied nothing mechanical was wrong with the aircraft. The IFS owns a copy of the official USAF accident report. |
31 October 1963 | F-104D | 57-1325 | 479TFW | USAF | incident | pilots ok |
This Starfighter encountered an accident at George AFB. Impact was low and aircraft could be repaired soon. One of the pilots was named Lougff. |
1 November 1963 | CF-104 | 12764 | 6STR-OTU | RCAF | written off | pilot ok |
7 November 1963 | F-104A | 4211 | 8TFS | RoCAF | incident | pilot ok |
9 November 1963 | F-104A | 56-802 | 9sq | PAF | written off | pilot ok |
It crashed after it went into a spin. F/O Asghar Shah ejected safely. (Note: It was not lost on 13 November) |
13 November 1963 | F-104C | 57-930 | 435TFS | USAF | incident | pilot ok |
It suffered failure of the left leading edge flap and in-flight extension of the MLGs following a rocket pass at Cuddeback Gun Range. He was able to land safely at Edwards AFB, California. The pilot was Capt Dayle W. Carlson of 479-TFW, 435-TFS. Mishap occurred on a 4-ship bombing, rocketry and strafing mission at Cuddeback Gunnery Range. Two nuclear weapons deliveries were practiced then on the first hot rocket pattern pass Capt Carlson fired a rocket at 2,000’ AGL and commenced a 4G recovery during which he heard a loud explosion and felt the aircraft yaw and roll to the left. The pilot immediately corrected and selected AB climbing to 10,000’ but the aircraft would not accelerate beyond 350 knots and 3-4,000’ per minute. During the climb the pilot noticed that the left leading edge flap had been torn free from its mounting hinge. At 10,000’ ft the pilot came out of AB and slowed to 300 knots then started towards Edwards AFB. The Flight Leader joined up with him and noted that both main gears were down, the forward starboard gear door was open, and the nose gear was retracted. Also, the left leading edge flap was laying obliquely across the left wing and still attached to the fuselage near the wing root by the drive mechanism. In addition, the left forward main gear door had been partially torn from the aircraft. The pilot slowed the a/c to 260 knots and selected gear down position. The Leader saw the nose gear extend and the remaining portion of the left forward gear door cycled to the partially closed position. Actuation of the doors could not be positively verified in flight but the pilot observed two green lights on the main gear indicators followed by a nose gear down indication. The Flight Leader recommended a no flap straight-in approach and the pilot elected to fly final to Edwards AFB Runway 22 at 240 knots. Touchdown was uneventful, the drag chute deployed, and the a/c taxied to the de-arming area where the pilot disembarked without injury. The IFS owns a copy of the official USAF accident report. |
21 November 1963 | F-104G | FX27 | SABCA | BAF | written off | pilot ok |
This brand new Starfighter crashed before delivery to the Belgium Air Force, at Sart-Dames Avelines (near Gosselies) after the pilot encountered a flame out at 650 feet. The pilot, Bernard Neefs (SABCA) ejected safely. Insurance-wise this FX27 was replaced by a new one lateron which got the same serial. Picture of the wreck at the crash site thanks to Charles Mali. |
![]() |
26 November 1963 | F-104A | 56-849 | 331FIS | USAF | incident | no pilot |
26 November 1963 | F-104A | 56-863 | 331FIS | USAF | written off | pilot killed |
26 November 1963 | F-104A | 56-866 | 331FIS | USAF | incident | no pilot |
4 December 1963 | F-104G | 61-2606 | 4333CCTS | USAF | written off | pilot ok |
10 December 1963 | NF-104A | 56-762 | ARPS | USAF | written off | pilot ok |
15 December 1963 | F-104A | 56-818 | 331FIS | USAF | written off | pilot killed |
18 December 1963 | F-104A | 4208 | 8TFS | RoCAF | written off | pilot killed |
1963 | F-104A | 4221 | 8TFS | RoCAF | incident | pilot ok |
Somewhere this year this aircraft landed just 50ft short of the runway. It then pulled up and came down again after 600meters. Because the main gear was completely lost it glided over 8000ft runway before it stopped aside the runway also loosing its nosewheel. It was repaired and continued operations soon after. Pilot was ok. |
##
Back to accidents overview |
Copyright © 2025 I-F-S.NL Protected by U.S. and International law for the F-104 Society Inc. The Netherlands | Developed by Media4ever and Ralphdesign