5 January 1962 | F-104A | 56-864 | 157FIS | SC ANG | written off | pilot ok |
This F-104A crashed 13 miles from its alternate field Rota NAS Spain after running out of fuel during very bad circumstances (heavy fog). It suffered an engine flame-out due to fuel-starvation while diverting to an alternate landing field. The pilot, 1Lt Clifton M. McClure, was forced to eject and survived with no injuries. The aircraft was destroyed. The pilot took off from Moron AB, Spain at 0914 local time for an FCF of the internal auxiliary fuel tank following an aux fuel tank float valve replacement the night before. The FCF was accomplished quickly within less than 10 minutes and then the pilot had requested a practice intercept against two other scheduled F-104s. The weather was briefed as VFR all day. At this time the aircraft was taken over by GCI and completed several intercept attacks. At approximately 0955 the 157-FIS Operations Officer called all aircraft back as weather appeared to be closing in on Moron. At 1007 the pilot was vectored back to Moron for recovery. The pilot had Moron in sight but there was traffic (a VC-97 aircraft). Lt McClure could see the clouds moving in over Moron. A departing C-124 reporting entering clouds out of Moron at 100 ft with fog. The VC-97 landed and reported thick fog on the runway. This F-104 entered the top of the clouds inbound and descended into solid cloud. He executed a missed approach. He reported the field (Moron) as below minimums and was diverting to Rota Naval Air Station. At no time did any control agency notify Lt McClure of the rapid and complete weather deterioration at Moron. Lt McClure turned towards Rota and for the next 6 minutes participated in 30 radio transmissions all of which were for the purpose of obtaining GCA frequency for Rota which he believed must have also gone IFR as suddenly as Moron. At 1021 the pilot established contact with Rota GCA and reported at 11,000 ft on emergency fuel with IFF on all three modes. Rota GCA ordered descent to 1,500 ft (he was still on top of continuous cloud deck) with 300 lbs fuel remaining. Rota GCA was never able to make contact with 56-864’s IFF and on two occasions instructed him to go standby, with no pickup results. At 1025 Lt McClure saw the coastline, and sand dunes with scattered clouds and just 150 lbs fuel remaining. He questioned a 270 degree vector given by Rota GCA which he saw would put him over the Atlantic Ocean. He continued on a 200 degree heading until his engine flamed out. The pilot ejected successfully. The aircraft crashed in a marshy area 13 NM North of Rota and the debris, which remained above water, indicated that the aircraft was on a direct heading to Rota. The IFS owns a copy of the official USAF accident report. |
16 January 1962 | F-104C | 57-924 | 436TFS | USAF | written off | pilot ok |
This Starfighter crashed shortly after takeoff from Luke AFB. Pilot Major Robert A Menke ejected and sustained minor injuries. Cause of the accident was a fuel shut off valve closure, resulting in a modification procedure later on for all F-104s. He flew from Luke AFB to George AFB together with Capt Lawrence Know with 56-922. Take off was normal but 5 to 10 seconds after coming out of afterburner pilot Menke experienced a muffled explosion similar to that of a compressor stall. He immediately checked his engine instruments and airspeed and noticed that his engine RPM was rapidly decreasing and his forward speed was decelerating to gliding airspeed. At 70 percent RPM he stop cocked the engine and initiated a stall clearing procedure and advanced throttle to the full mil position. The result was negative, just as a second attempt. By that time the altitude has dissipated to appr 1700 feet indicated. He jettisoned his external fuel tanks. He did two attempts to relight the engine which failed. Airspeed was well below 200 knots and RPM was 30 pct. Finally Major Menke ejected safely at approximately 700 feet above the terrain. Findings: Materiel failure or malfunction of the main fuel shutoff valve due to unknown cause. Recommendations: That all F-104 aircraft be given a one-time inspection to insure that the main fuel shutoff valve is operating within the prescribed T.O. limits. That guard over the switch be safetied in the on position and presently installed switch guard spring lock be removed. The IFS owns a copy of the official USAF accident report. |
16 January 1962 | CF-104 | 12703 | CEPE | RCAF | incident | pilot ok |
17 January 1962 | QF-104A | 56-745 | 3205DS | USAF | written off | no pilot |
This aircraft was written off as drone this day. It was owned by the 3201st Maintenance Group within the AFSC Eglin. It was the first QF-104A loss of the drone-unit. During an unmanned testflight it encountered an elevator malfunction and crashed on take off. The aircraft was totally destroyed. Note : In total the aircraft had re-gistered 2 successful unmanned missions before. |
18 January 1962 | F-104D | 57-1318 | AFSC | USAF | incident | pilots ok |
25 January 1962 | F-104F | BB+366 | WS10 | GAF | written off | 1 pilot killed |
(USAF serial 59-5000) This F-104F crashed near Oberbolheim after it encountered an afterburner failure during take-off from Norvenich. Hptm Lutz Tyrkowski was killed and Olt Horst Volter ejected and was safe. Despite the afterburner 'stopping' the pilots decided to continue their take-off although not reaching enough height. Following eye-witnesses the F-104 flew over houses nearly touching the roofs and strucking some poplar-trees. Then it went "trough" a factory on the 1st floor. Shortly before entering the building pilot Volter (student) managed to eject out of the aircraft and was safe. |
29 January 1962 | F-104B | 57-1311 | 157FIS | SC ANG | written off | 1 pilot killed |
1 February 1962 | QF-104A | 55-2963 | 3205DS/AFFTC | USAF | written off | no pilot |
3 March 1962 | F-104B | 4104 | 8TFS | RoCAF | written off | pilots killed |
(USAF serial 57-1299) This two-seater crashed South of the runway during the landing at homebase CCK (Ching Chuan Kang) in Taiwan after encountering a flameout. The aircraft ran out of fuel which was not noticed due to a malfunctioning measuring system, resulting in a sudden flame-out. The crew attempted to make an emergency landing but failed. Sadly it was too late, they were too low. The front seat pilot, Capt Ku Chen-Hua (31), made no attempt to eject. The rear seat pilot, Col Li Shu-Yuan (38), ejected at low altitude, but did not separate from the seat (too late and too low). This failure was due to maintenance, because the separation harness was not connected to the seat. |
19 March 1962 | F-104A | 56-813 | 151FIS | Tenn ANG | written off | pilot killed |
19 March 1962 | F-104A | 56-848 | 151FIS | Tenn ANG | written off | pilot killed |
21 March 1962 | F-104A | 56-881 | 151FIS | Tenn ANG | written off | pilot ok |
22 May 1962 | CF-104 | 12707 | 6STR-OTU | RCAF | written off | pilot ok |
22 May 1962 | F-104G | DA+107 | JBG31 | GAF | written off | pilot ok |
(c/n 2029). This Starfighter crashed shortly after take-off from homebase Nörvenich at Mersch near Jülich after engine an failure due to loss of pressure in the fuel system. This resulted in the closure of the Inlet Guide Vanes (IGV). Pilot Olt Siegfried Heltzel ejected safely but was badly injured, The aircraft was in use from march 8th, so only 2 months old. |
2 June 1962 | F-104A | 56-862 | 157FIS | SC ANG | written off | pilot ok |
This Starfighter crashed near Cordoba, Spain following an engine failure. The pilot was 1Lt Stanley L. Hoke of 157-FIS, USAFE, Moron Air Base, Spain, safely ejected. He flew this day at 17:57 local on a practice scramble mission from the alert hangar at Moron Air Base, Spain. It was on a 15 minute alert status. Pre-flight and take-off were normal except the pilot noticed no cabin pressure after t/o. The first 40 minutes of the flight were normal. During the flight the highest altitude reached was 27,000 ft, but since the cockpit pressurization was out intercepts were performed at 19,000 ft with Lt Hoke acting as the target. After the intercepts had been completed Lt Hoke attempted to join up with the lead aircraft. While joining he slightly overshot so he extended the speed brake and reduced power to just above idle. Immediately after he felt an intermittent deceleration and observed RPM to be low at 65%. He advanced the throttle to Military but the RPM did not increase. Lt Hoke then activated both airstart switches and heard the ignition, but the RPM remained at 65%. He stop cocked the throttle and activated the start switches again. As the RPM passed 50% he advanced throttle to Military but again the RPM hung up at 65%. He retracted the speed brakes and the RPM gradually decreased from the high of 65%. Shortly thereafter both generators cut out. He extended the RAT and attempted more airstarts. The RPM then began to hang up at 53% when advancing to Military power.Lt Hoke lowered take-off flaps and established a glide of 240 knots attempting more airstarts. He noticed fuel flow to be 250 to 350 PPH and TPT around 500 degrees C. At one time the fuel flow was 500 PPH and TPT 300 degrees C, although both gauges kept dropping back to 200 to 300 PPH and 300 degrees C. Continuous airstarts produced the same results with RPM slowly decreasing to just 36%, fuel flow at 250 PPH, and TPT around 250 degrees C. Overall, 7 or 8 stall clearings were attempted. The pilot also activated the IGV switch and throttled into AB as a last resort. Passing through 5 or 6,000 ft, Lt Hoke successfully ejected after leaving the throttle in full military power with RPM indicating 36%. The pilot did not jettison the canopy before pulling the ejection ring. Lt Hoke landed safely about 2 miles from aircraft impact and about 5 miles from La Carlota. The aircraft crashed 8 nautical miles SSE of Cordoba, Spain. The F-104 dived to the ground near vertical, exploding on impact. Most of the wreckage was contained in a hole the width of the wings. Excavating the remains of the aircraft necessitated digging thirty to thirty-five feet down. Investigation: Primary factor: technical: main fuel control, Materiel failure or malfunction of main fuel control or failure of main fuel shut-off valve to the closed position. The IFS owns a copy of the official USAF accident report. |
18 June 1962 | F-104A | 56-809 | 197FIS | Ariz ANG | written off | pilot ok |
19 June 1962 | F-104F | BB+365 | WS10 | GAF | written off | pilot killed |
19 June 1962 | F-104F | BB+370 | WS10 | GAF | written off | pilot killed |
19 June 1962 | F-104F | BB+385 | WS10 | GAF | written off | pilot killed |
19 June 1962 | F-104F | BB+387 | WS10 | GAF | written off | pilot killed |
12 July 1962 | F-104A | 4207 | 8TFS | RoCAF | written off | pilot killed |
31 July 1962 | F-104A | 56-759 | AFSC | USAF | incident | no pilot |
10 August 1962 | QF-104A | 56-734 | 3205DS | USAF | incident | no pilot |
While returning from an unmannend test flight, this drone 56-734 "QFG-734" engaged the barrier on landing because it encountered braking problems. Everything went fine and there was no damage. The aircraft was checked and available soon for new drone operations. |
10 August 1962 | CF-104 | 12742 | 6STR-OTU | RCAF | written off | pilot killed |
This Cold-Lake based plane crashed during a touch and go due to loss of thrust. The pilot, FlLt. Jake R. Mulhall ejected but sustained fatal injuries when his parachute disintegrated in the aircraft fire area and was sadly killed. The cause was an oilpump failure. The pilot ejected just after lift-off during the touch and go at Cold Lake. Because there was almost no wind, the parachute came down straight and landed into the middle of his fireball with the chute vaporizing above the ground. The IFS owns a copy of the accident report of this terrible accident. |
16 August 1962 | F-104C | 56-912 | 479TFW | USAF | incident | pilot ok |
It encountered an accident at Tyndall AFB but could be repaired lateron. Pilot, 1st Lt John L. Mesenbourg was ok. Together with aircraft 57-923 (Lt Korcheck) both were supposed to fly back to George AFB after participating in Operation Firefly at Tyndall AFB. There was a fuel stop planned at Cannon AFB, Nw Mexico. Two minutes after takeoff Lt Mesenbourg reported problems with no 1 Generator switching on and off. Soon later this was followed by hydraulic problems with stuck gauge and losing communication (radio) and now a double generator failure. He decided to return back to Tyndall and make an emergency landing. Since he did not burn extra fuel to lower the landing weigth he came in to hard, chute broke, brakes could not decelerate sufficient and aircraft entered the barrier system. It failed catching the barrier and aircraft continued through the overrun onto the dirt for some distance when the nose gear collapsed and farther on the right tip tank and wing struck a concrete post adjacent to the ILS trailer which caused a fire. It came to rest 1203 feet from the end of the overrun. The pilot evacuated the aircraft unhurt. The damage was substantial but could be repaired. The IFS owns a copy of the official USAF accident report. |
21 August 1962 | F-104C | 56-935 | 476TFS | USAF | written off | pilot ok |
25 August 1962 | F-104D | 57-1328 | 479TFW | USAF | written off | pilot ok |
3 September 1962 | F-104G | DA+116 | JBG31 | GAF | written off | pilot killed |
4 September 1962 | CF-104 | 12803 | Canadair | RCAF | written off | pilot ok |
This Canadair factory, Montreal owned aircraft hit some trees on final approach and crashed near Montreal. The pilot, FlLt. L. S. Lumsdaine ejected safely. Some components of this aircraft, which was on its acceptance flight, were used inside the currently displayed ColdLake gateguard '12872'. |
7 September 1962 | QF-104A | 56-734 | 3205DS | USAF | incident | no pilot |
Just as on August 10th, this drone Starfighter encountered problems during the landing after an unmanned test flight. It engaged the barrier after returning to the airbase and again his time there was no damage and everything went ok. It returned soon back to operational drone operations. |
10 September 1962 | F-104D | 57-1325 | 479TFW | USAF | incident | pilot ok |
This day this F-104D encountered an incident on the ground at George AFB but the aircraft could be repaired soon. The incident was very light, a reason why the USAF did not initiate an official accident/incident report. |
12 September 1962 | QF-104A | 56-734 | 3205DS | USAF | incident | no pilot |
14 September 1962 | QF-104A | 55-2968 | 3205DS | USAF | written off | no pilot |
On this day QF-104A 55-2968 "QFG-968" was lost in the Gulf of Mexico. It was flying its second unmanned flight, which ended tragically without understanding the cause. Likely the system lost control of the aircraft. |
4 October 1962 | QF-104A | 56-736 | 3205DS | USAF | written off | no pilot |
This QF-104A "QFG-736" was shot down by a missile on purpose during shooting exercises. It was its 5th and also last unmanned flight. The aircraft crashed into the ocean in a secured area. |
10 October 1962 | F-104C | 56-920 | 476TFS | USAF | written off | pilot ok |
20 October 1962 | F-104C | 56-903 | 476TFS | USAF | incident | pilot ok |
20 October 1962 | F-104C | 56-922 | 476TFS | USAF | incident | pilot ok |
This F-104C suffered a right MLG failure and landing accident at Key West Naval Air Station in Florida on a 479th TFW deployment. The pilot was not injured but the aircraft was significantly damaged. The pilot was Captain James J. Torson with 479 TFW, 476 TFS. On the second wave of 10 F-104s on deployment to Key West NAS, Florida Captain Torson flew element lead with 1Lt Hauth as wingman. The mission included two air-refueling. Lt Hauth experienced pylon tank feeding problems and these two aircraft diverted twice, once to England AFB, later to Tyndall AFB. During the flight from Tyndall to Key West NAS the UHF radio failed in Lt Hauth’s F-104. Because this was to be a strange field night landing with his wingman’s radio out, Capt Torson elected to land in formation. A radar penetration and GCA formation landing were made at Key West NAS. At touchdown the right main landing gear of Capt Torson’s F-104 failed and the aircraft settled onto the right pylon tank. Lt Hauth, on Torson’s right wing in formation, went into afterburner, accelerated and passed on the right hand side of Capt Torson and stopped without incident. Capt Torson continued down the runway in 56-922 drifting to the right and departed the runway at the 4,000 ft mark. The nose gear sheared approximately 400 feet after leaving the runway. The left MLG did not fail. The F-104 travelled approximately 1,000 feet after leaving the runway, coming to rest 20 feet from a lagoon. Aircraft could be repaired soon again. Findings: Materiel failure. Failure of drag strut pin boss hole resulting in failure of main landing gear. Recommendations: That a design engineering study be initiated to determine if the F-104 landing gear can or need be improved to withstand greater landing stresses in view of the rework to be accomplished in TO 1F-104-837. Final fix: Special depot teams have been dispatched to all F-104 squadrons. All main landing gears are being reworked on the spot to provide adequate radii of the blind hole for the drag strut attaching pin. The IFS owns a copy of the official USAF accident report. |
20 October 1962 | F-104C | 57-929 | 476TFS | USAF | incident | pilot ok |
This F-104C suffered a broken refueling probe during inflight refueling from a KB-50J tanker at 22,000’ near Hobbs, New Mexico. The broken probe lodged in the horizontal stabilizer and could not be dislodged. A safe landing was made at Webb AFB, TX. The pilot was not injured. The pilot was 1Lt Robert H. Jones with 476-TFS, 479-TFW. This mishap occurred during a CASF (Composite Air Strike Force) deployment from George AFB, California to Key West NAS, Florida with two aerial refuelings enroute. This flight consisted of ten F-104Cs led by LtCol Rosenbaum and made a normal rendezvous for the first aerial refueling normally at a point 10 miles east of Hobbs, New Mexico. All 10 F-104Cs hooked up to the KB-50J tankers at 22,000 ft in moderately turbulent air. As the fuel load in the F-104Cs increased, several pilots experienced stick shaker actuations. Just before Lt. Jones received his full fuel load the stick kicker moved the stick forward and held it there for 2 to 3 seconds. The nose of the aircraft dropped sharply and the forward portion of the refueling probe broke off. This loose section of probe became lodged in the leading edge of the horizontal stabilizer. The stick then returned to neutral momentarily and then moved again to the kicked position for another 2 to 3 seconds. The stick returned to neutral and Lt Jones noted his airspeed was 240 KIAS, his angle of attack reading .3 and his altitude 2-3,000 ft below the tanker formation. Lt Jones informed the flight leader that his probe had broken off and he was diverted to Webb AFB, Texas with his element leader Captain Delashaw. During the flight to Webb AFB, Lt Jones tried to dislodge the probe from the stabilizer without success. He was able to land safely at Webb AFB without incident using a straight in approach. Total duration of flight was 3 hours. Aircraft was operational again soon. The IFS owns a copy of the official USAF accident report. |
23 October 1962 | F-104A | 4222 | 8TFS | RoCAF | written off | pilot ok |
(USAF serial 56-800) While approaching home base CCK for landing this Starfighter crashed after it lost engine power and an engine stall at 7000ft. The pilot, Chu Wei Min, tried some restarts (fuelflow became 0) and after this was not succesful he ejected at 3000ft and was safe. The aircraft crashed and was totally destroyed. |
8 November 1962 | F-104F | BB+368 | WS10 | GAF | incident | pilots ok |
17 November 1962 | F-104A | 4213 | 8TFS | RoCAF | incident | pilot ok |
(USAF serial 56-777) On this day this F-104 was seriously damaged. Pilot Chuan Ren-Lian was not Injured and the plane could be repaired. |
10 December 1962 | F-104B | 57-1310 | 157FIS | SC ANG | incident | pilots ok |
This F-104B received major damage when both main gears collapsed on initial takeoff roll from McEntire ANGB, South Carolina. There was no injury to either pilot. The pilots were Captain Clifton M. McClure and 1Lt James Altman both with South Carolina ANG, 157-FIS. Scheduled as an Air Defense mission acting as a target, this aircraft lined up for takeoff at McEntire ANG base. Minimum AB was selected and almost simultaneously as the AB lit and the brakes were released, a loud noise was heard and the left wing started settling and the aircraft began veering left. Lt McClure throttled back to idle RPM then immediately shut down the engine when he realized the left wing was settling lower then a blown tire would normally allow. Both pilots evacuated the aircraft without injuries. The aircraft received major damage when both landing gears had failed allowing them to contact the pressure bulkhead immediately aft of the main gear. Findings: Materiel failure. The left main gear drag strut assembly failed. Final fix: TOC1F-104-841 (publ. 11-12-1962) Inspection and rework of main landing gear drag strut. The IFS owns a copy of the official USAF accident report. |
13 December 1962 | QF-104A | 56-796 | 3205DS | USAF | written off | no pilot |
This day this QF-104A "QFG-796" sheared its nose-gear on landing, left the run-way, rolled over and burned. This was the end of 56-796 which just returned from its first unmanned flight. It was totally destroyed/burned and subsequently the remains were scrapped. |
20 December 1962 | F-104A | 56-749 | ATPS | USAF | written off | pilot ok |
21 December 1962 | F-104C | 56-924 | 476TFS | USAF | written off | pilot killed |
1962 | F-104D | 57-13.. | 479TFW | USAF | incident | pilots ok |
Summer or fall of 1962. An F104D with teacher Carnahan and German student Hfw Gert Poelchau made an emergency landing at Edwards. During flight with Mach2 which was needed to get a nice charter, the aircraft wanted to turn lightly over its yaw-axis and the student immediately shut off the afterburner. Carnahan asked Poelchau if he had played with the trimming, which was not the case. After finding out another strange thing both pilots decided to land as soon as possible. After landing they were shocked by finding out what happened. At the nozzle-ring a fin was broken off and a big hole was melted inside the back of the aircraft. Half of the rudder was also missing while parts of the vertical stabilizer were burned! The pilots went back to homebase George by a C130. The aircraft could be repaired soon and no official USAF accident report could be found. Aircraft identity and date in 1962 stay unknown. |
1962 | F-104C | ????? | 436TFS | USAF | incident | pilot ok |
This unidentified F-104 encountered an incident somewhere in 1962. The pilot Max Jersperon was fine. He stated later: “Many test-hops turn out to be more exciting than planned. I was on a test-hop in an F-104 out of George AFB. Normal test would be an afterburner climb to 37,000 feet and accelerate to mach 2, checking all systems and instruments, recovering with a simulated instrument approach GCA/ILS. I was cleared #1 on the runway, and began my take-off roll, with the nose wheel lifting off at 180 knots, and then airborne at 210 in under 3,000’ of runway. Sucked the gear up, then boom, the aircraft blew up – at least I thought it did. The plane went in to severe buffet only a few feet off the runway. Noticed the runway going by underneath, the hatch had departed the aircraft (downward ejection). All preflight checks had indicated a safe hatch. I pulled up onto a downwind leg, and was unable to contact the tower as the UHF antenna is in the hatch. Fortunately, there were no aircraft on initial approach. The flight lasted about five minutes.” Sadly nothing more is known.. Glad to understand that the aircraft and pilot were both safe. |
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