23 January 1961 | F-104C | 56-931 | 435TFS | USAF | incident | pilot ok |
9 February 1961 | F-104A | 56-761 | ARDC | USAF | written off | pilot ok |
2 March 1961 | F-104C | 56-922 | 434TFS | USAF | incident | pilot ok |
This F-104 experienced loss of oil pressure and a nozzle stuck wide open shortly after take off and climb out. An emergency landing was made at George AFB but the aircraft departed the runway on landing roll shearing off all of the gear. The pilot 1Lt Richard Keith Clements, was not injured. Accident occurred during 3-ship aerial tactics training with Lt Clements as No. 2 in 56-922, Lt Linihan as Lead in 57-922, and Lt. King as No. 3 in 56-927. Shortly after single ship takeoffs the formation joined in a climbing left turn at 7,500’. Then as a climbing right turn was initiated Lt Clements noted the following instrument readings: EGT 600 degrees, 40 PSI oil pressure, 104% RPM. The formation was at 22,000’ MSL and Lt Clements had to reduce throttle to idle and use speed brakes to keep from over-running the formation. No.3 in trail noticed that Lt Clements nozzles were wide open. The EGT of Lt Clements aircraft with throttle at idle was 375 degrees. Lt Clements flew on Lead’s wing to a low key position for a landing from an SFO pattern. At low key Lt Clements noted his RPM was 100%, EGT 375 and oil pressure 40 PSI. The aircraft was configured with gear down, take off flaps down, speed brakes in, throttle in idle, airspeed 240 KIAS. When manipulating the throttle from idle to Military there was little thrust change. Lt Clements turned a wide base leg and airspeed increased to 260 KIAS during the descending turn. He crossed the overrun at about 210 KIAS and touched down at approximately 200 KIAS. A good touchdown was made 500’ from the approach end and center of Rnwy 21. At 170 KIAS the drag chute was deployed, blossomed, and then failed. At 2,200’ remaining the right main tire blew. The pilot noted 150 knots as he went by the 2,000’ remaining marker. He attempted to steer to the center of the barrier but departed the right side of the runway approximately 500’ short and 33’ right of the barrier. At some point the main and nose gear failed. The F-104 continued 1,290’ beyond the end of the runway and came to rest 90 degrees to the runway heading. Fuel on board was 5,500 lbs. The pilot evacuated the aircraft immediately when it came to rest. He was not injured. The engine was still running and stop cocking the throttle did not cut the engine. After the main fuel cut-off switch was deactivated the engine windmilled down. The International F-104 Society owns a copy of the official accident report. |
13 March 1961 | F-104A | 56-859 | 157FIS | SC ANG | written off | pilot ok |
17 March 1961 | F-104A | 56-819 | 151FIS | Tenn ANG | written off | pilot ok |
This Starfighter crashed 1.5 miles NNE from Rockford, 3.5 miles from home base McGhee-Tyson Apt, Tennessee. Pilot Major Robert Andrew Bennett was ok. He departed from McGhee on a functional check flight following an engine change. Immediately after takeoff, the gear control handle would not come out of the down position. The pilot limited the speed to try to get the gear up manually which succeeded. To assure that everything was ok he repeated gear down and up with the gear handle. As the gear retracted again the pilot experienced a loud thump, followed by a rise in EGT and a loss of RPM. The sound was not from the closing doors. The engine did not react anymore on the throttle and the pilot decided to eject when he noted the EGT at 950 degrees. His flight took 1 minute and 14 seconds from start to ejection. The pilot sustained no injuries, the aircraft was destroyed by impact and fire. The International F-104 Society owns a copy of the official accident report. |
29 March 1961 | F-104F | BB+375 | WS10 | GAF | written off | pilots ok |
7 April 1961 | F-104A | 56-757/757 | ChinaLake | US NAVY | written off | pilot killed |
9 April 1961 | F-104A | 56-781 | 197FIS | Ariz ANG | written off | pilot killed |
This F-104A crashed 7 NM WSW of Phoenix Apt, Arizona on a radar interception mission on a T-33, as leader of a 2 ship formation. Pilot Maj Erich Julius Hettlinger was sadly killed while ejecting with his ejection seat. After pilot Hettlinger experienced radio difficulty the mission failed, both lost visual contact with each other, and both returned back to the airbase separately. While flying an approved penetrating CGI on return the pilot experienced malfunctioning speed brake control. One minute later he experienced having only 80% RPM. He was at 3500 feet and descending fast. Before ejecting he was advised to assure he was above unpopulated area. Then he declared a low-oil failure. Soon after the aircraft was seen crashing into a dry river bed without noticing a chute. The pilot ejected sadly unsuccessfully. The seat was found apart from the impacted aircraft. The IFS owns a copy of the official accident report. |
5 May 1961 | F-104A | 56-855 | 151FIS | Tenn ANG | written off | pilot killed |
This F-104A crashed 3 miles NE Alcoa, Knoxville Tennessee, near McGhee Tyson AB. Pilot Capt. Luciano Guida (transition pilot from the Italian Air Force for the AFFTC Edwards AFB) was sadly killed in this accident. It all happened on his 12th flight in his F-104 transition program. Major R.B. Weinard was the leader of the twin flight. During the formation take off roll, Capt Guida did not get een afterburner light and he was informed by the mobile control but sadly did not acknowledge this (perhaps due to radio problems). He continued the takeoff and left the runway and crossed the overrun in a nose high attitude with the tail dragging. He maintained the attitude for 450’ beyond the overrun where he bounced briefly into the air for 170’ and then contacted the ground hard in a porpoise with all three gear for 360. He then bounced into the air again for 150’ and then his right wing dragged the ground for 120’ as he passed the ILS antennae. He again bounced into the air for another 300’ hitting the top of the 5’airport boundary fence which is 1800’from the end of the runway and continuing another 150’into an adjoining field. He lost the ventral fin and engine blow out panel and the ILS antennae. It went airborne again for 800’ clearing a deep ravine and then landing tail first.. At this point the aircraft began disintegrating. The canopy was found 200’ beyond the ravine so it would appear the pilot ejected between the ravine and the canopy. Aircraft was disintegrated and burned. Pilot did not have a change and was found near the seat in which he had ejected. It was a very tragic accident. Note: Capt Luciano Guida was undergoing type conversion with the Tennessee ANG and was selected for the Joint Test Force. It was his last flight at Knoxville, Tennessee. His place was taken by Capt Bonazzi.The IFS owns a copy of the official accident report |
5 May 1961 | F-104C | 56-885 | 476TFS | USAF | written off | pilot ok |
5 May 1961 | F-104B | 4102 | 8TFS | RoCAF | written off | pilots killed |
13 May 1961 | F-104C | 56-884 | 476TFS | USAF | written off | pilot killed |
22 May 1961 | F-104D | 57-1329 | 479TFW | USAF | incident | pilot ok |
25 May 1961 | F-104D | 57-1330 | 435TFS | USAF | incident | pilots ok |
This F-104D suffered a landing accident at Wright-Patterson AFB, Ohio due to nose-wheel shimmy. Damage was minimal and the crew were safe. Pilots were LtCol Harold E. Collins (Pilot AFSC/ASD Fighter Ops Div at Wright-Patterson) and Capt Kenneth D. Ohman (Instructor Pilot 479TFW/435TFS). They were both on a TAC directed mission to flight test the refueling probe with the KC-135 probe-drogue adapter system. The aircraft was on temporary loan to Fighter Ops Div, Directorate of Flight Test, Wright-Patterson AFB. This day at 1215 hours, the aircraft participated in these tests with LtCol Collins in the front seat and Capt Ohman in the rear. The test portion of the mission was completed in routine fashion, and there was no nose-wheel shimmy on take-off. During landing with approximately 3,000 lbs of fuel remaining, touchdown was made at 155 KIAS at Wright-Patterson, the nose wheel was lowered and nose wheel steering engaged. Severe nose-wheel shimmy developed and nose wheel steering was disengaged. The nose wheel continued to shimmy. To correct shimmy the nose was raised and held off the runway as long as possible. When the nose wheel again contacted the runway the drag chute was deployed. Severe nose wheel shimmy continued with or without nose-wheel steering engaged. Nose wheel steering then failed completely and the aircraft was turned off the runway by using differential braking. It came to rest safely, there was no injury to the crew. Downlocks were inserted, the aircraft was shutdown, and towed to the parking area. Duration of flight has been 2 hours 5 minutes. The IFS owns a copy of the official accident report. |
25 May 1961 | F-104A | 56-853 | 157FIS | SC ANG | written off | pilot killed |
15 June 1961 | F-104C | 56-897 | 476TFS | USAF | written off | pilot ok |
While on deployment in Spain this Starfighter crashed 2 NM East of El Coronil, 6 NM South of Moron AB. Pilot Lt. Larry Moench Davis ejected and was ok. He flew a practice scramble intercept mission with Capt. Huffman as lead. After a normal takeoff, as Lt Davis moved his throttle out of afterburner into military position, he felt and heard a chug or thump accompanied by a vibration and a noticeable loss of thrust. His nozzle was full open and oil pressure was around 20psi. Assuming a nozzle failure he pushed the throttle into afterburner trying to light the afterburner. This was unsuccessful. Capt Huffman informed him to pull the emergency nozzle closure handle. This went fine and RPM was 70%. However he did not experience increase of thrust and RPM was limited to 70%. The 104 was now very slow, low and descending and stick shaker was operating. He was advised to eject and this went fine. The aircraft crashed into a hillside and exploded, scattering wreckage for about a quarter of a mile in the line of the flight. Lt Davis landed about 300 yards from the aircraft and was unhurt. He was picked up by a helicopter and returned to Moron AB. The IFS owns a copy of the official USAF accident report. |
16 June 1961 | F-104C | 56-932 | 436TFS | USAF | incident | pilot ok |
This Starfighter encountered an accident after takeoff from George AFB but could be repaired afterwards. Pilot Lt. William Thornton Smith was ok. It departed George with another F-104C to fly to the Cuddeback shooting range on a practice mission for an aerial demonstration which was to be conducted as part of the Falcon 61 project. Upon arrival, appr 15 miles W of the range, both aircraft assumed appr 15 seconds spacing and started a shallow dive towards the range. They had to pass over the range supersonic and pull up to intercept a T-33. During the dive the pilot selected full afterburner and crossed the special weapons target at 1350 feet with 650kts. As the lead pilot began to pull up he experienced what he interpreted to be a severe compressor stall. He immediately performed the stall clearing procedure and obtained to restart which was successful. While climbing to 20000 feet he noted that both leading edge flaps were missing.. At 20000 feet he successfully extended the trailing edge flaps to the take-off position. While slowing to 220kts he encountered severe buffeting and declared an emergency, heading for Edwards AFB. The wingman told him that both main landing gear were extended, doors were missing and the nose gear was retracted. The leader then noted that the gear handle was “up”. However both main gear green lights were on, signifying that gear to be up and locked. He placed the handle to the down position and the nose gear seemed to extend normally, indicating down and locked. No fluid was noted streaming from the aircraft so the pilot made a successful straight-in landing at 240kts including a good working chute. The IFS owns a copy of the official USAF accident report which is sadly not clarifying the exact cause. |
26 June 1961 | F-104C | 56-923 | 436TFS | USAF | written off | pilot killed |
26 June 1961 | F-104C | 57-917 | 436TFS | USAF | written off | pilot ok |
2 August 1961 | F-104C | 56-893 | 476TFS | USAF | written off | pilot killed |
This F-104C crashed 44 NM SE of Moron, 3 NM E of town Jubrique in Spain during a deployment. Pilot 1st Lt Johny Lee King was sadly killed. That afternoon 4 aircraft flew a 2 to 2 intercept and simulated air combat training mission. Pilots were Lt Tamm, Lt Plummer, Major Loeffler and Lt King. Lt Tamm and Lt King were the flight leaders. During this mission on one moment the other three aircraft lost contact with Lt King. It was just after they had been in a steep dive attitude. Then Major Loeffler noted smoke behind and below him on the ground and saw that this was the aircraft of Lt Kind who had crashed. The cause of the accident is unknown but could well have been caused by loss of control of the aircraft due to disorientation or technical failures. It crashed approximately 18 minutes after takeoff. The IFS owns a copy of the official USAF accident report. |
5 August 1961 | F-104B | 57-1306 | 151FIS | Tenn ANG | incident | pilots ok |
11 August 1961 | F-104C | 56-899 | 436TFS | USAF | incident | pilot ok |
28 August 1961 | F-104C | 56-913 | 434TFS | USAF | written off | pilot killed |
31 August 1961 | F-104B | 57-1307 | 151FIS | Tenn ANG | incident | pilots ok |
This F-104B suffered a landing accident and was damaged at Campbell Army Air Field (Fort Campbell), Kentucky. Both pilots escaped without injury. The crew was IP Captain Alvin R. Ruthstein and student pilot 1Lt Errol L. Johnstad, both of ANG/ADC, 134-FG, 151-FIS, Tennessee ANG. The purpose of this flight was for Lt Johnstad to get his final dual ride prior to solo checkout. Take off from Berry Field (now Nashville IAP), Tennessee was normal and a touch and go landing was made on Rnwy 31 at Berry Field. Airspeed was at 175 knots on the rollout but as the aircraft crossed the runway threshold about 30 or 40 feet in the air both pilots stated that the rate of sink became excessive. Both pilots pulled back on the stick and throttled to Military but the aircraft struck the runway hard and bounced. Capt Ruthstein lit the afterburner and took the aircraft up and around. From this time forward Capt Ruthstein did all of the flying from the rear cockpit. Mobile control informed the crew that the right main landing gear had been damaged. Another F-104 was scrambled to check them over. This F-104 joined up and told the crew that the right main gear was broken off and dangling by the oleo strut. Capt Ruthstein decided to land at Campbell AAF (Fort Campbell, Kentucky) and requested the runway be foamed. When told this would take 25 minutes he decided not to wait and set up for landing. He burned fuel down to 600 lbs first. The F-104 touched down very light on the left main on Rnwy 22 at Campbell AAF, and the nose was lowered. The drag chute was deployed successfully and the right tip tank contacted the runway. Directional control was maintained with nose wheel steering for over 1,000 ft. As nose gear steering lost effectiveness the aircraft gradually turned right and departed the runway at the 3,200 foot mark. It continued another 400 ft ending up 90 degrees to the runway heading. The F-104 crossed a small ditch and collapsed the nose and left main gears. The pilots evacuated safely and there was no fire. Duration of flight was 6 minutes. The aircraft was repaired again. The IFS owns a copy of the official USAF accident report. |
6 September 1961 | F-104F | BB+378 | WS10 | GAF | written off | pilots ok |
7 September 1961 | QF-104A | 56-746 | 3205DS | USAF | incident | pilot ok |
7 September 1961 | F-104A | 56-811 | 151FIS | Tenn ANG | incident | pilot ok |
29 October 1961 | F-104C | 57-926 | 435TFS | USAF | incident | pilot ok |
This F-104C suffered a ground accident preparing for t/o roll at Ramstein AB, Germany when on deployment. The right main landing gear had apparently failed. There was no injury.Pilot was 1Lt George F. Tommasi with 435-TFS, 479-TFW. He was commencing take off on runway 27 at Ramstein AB, Germany for a 2-ship practice air defense mission. When full Military power was attained prior to take off the pilot heard a loud BANG and felt the aircraft settle onto the right wing. The pilot shut down because the aircraft was resting on the right pylon tank. The aircraft was removed from the runway without further incident and could be repaired. The IFS owns a copy of the official USAF accident report. |
14 November 1961 | F-104D | 57-1326 | 476TFS | USAF | incident | pilots ok |
On this day this F-104D departed the runway upon landing at George AFB, California. The crew was safe. The aircraft was piloted by 1Lt David H. Groark (student) and Captain Sam C. Henley (IP) both with 476-TFS, 479-TFW. This accident occurred following a normal, night checkout mission for Lt. Groark in the front seat (approx 1900 local time). Approach and letdown to Runway 16 at George was normal although one go around had been made when Lt Groark had lost too much altitude and airspeed on the first attempt to land. Downwind and base legs were adequate and the final approach looked good to mobile control, tower and both pilots until a point about 2,000’ from the end of the runway. At this point the IP (Capt Henley) told Lt Groark to add power and grabbed the stick himself. Immediately thereafter the aircraft struck the overrun approximately 780 ft short of the runway threshold. The F-104 bounced about 4 ft in the air and again touched down on the overrun when it then bounced up to and on the runway. The IP gained control and maneuvered the aircraft onto the runway with rudder. The IP attempted to maintain control with left brake when on the runway and the drag chute was deployed. The F-104 veered off the runway to the right and could not be controlled so the IP stopcocked the throttles. The aircraft departed the runway to the right 2,000 ft past the landing end, went down a slight decline and up a slight rise of sand where it came to a stop about 360 ft off the side of the runway at an angle of 60 degrees off runway heading. The 2 pilots abandoned the aircraft without incident. Duration of flight was 1 hr, 35 min. The IFS owns a copy of the official USAF accident report. |
21 November 1961 | F-104A | 56-756 | AFSC | USAF | incident | pilot ok |
25 November 1961 | CF-104 | 12712 | Canadair | CAF | written off | pilot ok |
27 November 1961 | QF-104A | 55-2966 | AFSC | USAF | incident | pilot ok |
9 December 1961 | F-104A | 56-841 | 157FIS | SC ANG | written off | pilot ok |
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