| 23 January 1961 | F-104C | 56-931 | 435TFS | USAF | incident | pilot ok |
| 9 February 1961 | F-104A | 56-761 | ARDC | USAF | written off | pilot ok |
| It crashed at the Buckhorn Dry Lake, 4 miles West of Edwards AFB. The pilot, Capt Albert Hanlin Crews jr. ejected safely. The aircraft from the ARDC toke off from Edwards AFB on a chase mission for an F-4H test flight. The aircraft rolled about 15 seconds after the F-4 and broke ground at appr 200kts. The gear handle could not be raised and repeated attempts failed. At 250 knots the throttle was retarded out of after burner and a definite bump or changeover occurred to confirm operation of the main engine only. Climb angle was increased slightly to reduce speed. The gear was retracted and the indicators were “up”. The throttle was advanced to the military power setting to accelerate the climb speed. On passing the runway control unit near the far end of the runway the exhaust smoke was reported to be darker or more dense than normal but the flame pattern was reported as normal for an after burner takeoff. The aircraft passed 500ft beyond mobile with the gear up at appr 800 feet altitude. Near the end of the runway a slight right turn was started to establish spacing relative to the F-4. The command radio was changed to the test frequency and the pilot started to raise take off flaps. Simultaneously a muffled boom was heard which the pilot said did not sound truly like a compressor stall. Airspeed was estimated to be 300 kts. Witnesses noted a very dark puff of smoke in the exhaust trail of the engine. A gradual loss of thrust was noted by the pilot. At 80 % RPM the pilot proceeded to break what he considered to be a compressor stall. The airstart switch was activated and the throttle was stopcocked, then moved to full throttle position (military). No response was noted. A second airstart attempt was also unsuccessful. About this time the pilot stated another “explosion” occurred. Witnesses observed a second dark puff of smoke about 500 feet beyond the first in the exhaust trail. The pilot noted no roughness in the engine before or after the explosions. Two additional clouds of smoke developed in very close sequence in the exhaust trail – perhaps 100 feet apart. Witnesses observed flames within the tailpipe as the aircraft reached the top of its arc. Then flames issues from the tail pipe thicker then the first followed by a very dense trail of smoke. The exact color of the smoke varied with the location of the observer. A witness on the ground south of the aircraft path described the trail being dark brown. A witness on the ramp, east of the trail described it as very dark. Airborne witnesses west of the trail described it as a contrail – white smoke. RPM dropped slowly through 80% but near 40% deceleration of the engine, seemed to drop faster. At this point with about 250 kts airspeed and 1000 feet of altitude but decreasing rapidly, the pilot realized that Rossmond Dry Lake was too far away for a flame out landing and he elected to bail out. The chute appeared to open around 500 feet altitude. A witness stated that the aircraft was trailing flames from the bottom of the tailpipe in a level altitude at the time of the ejection. Then it dove abruptly and crashed. Pilot was gladly unhurt. The International F-104 Society owns a copy of the official accident report. Photo beneath shows the aircraft in the period it was intensively used for air-air refueling testing. |
| 2 March 1961 | F-104C | 56-922 | 434TFS | USAF | incident | pilot ok |
| This F-104 experienced loss of oil pressure and a nozzle stuck wide open shortly after take off and climb out. An emergency landing was made at George AFB but the aircraft departed the runway on landing roll shearing off all of the gear. The pilot 1Lt Richard Keith Clements, was not injured. Accident occurred during 3-ship aerial tactics training with Lt Clements as No. 2 in 56-922, Lt Linihan as Lead in 57-922, and Lt. King as No. 3 in 56-927. Shortly after single ship takeoffs the formation joined in a climbing left turn at 7,500’. Then as a climbing right turn was initiated Lt Clements noted the following instrument readings: EGT 600 degrees, 40 PSI oil pressure, 104% RPM. The formation was at 22,000’ MSL and Lt Clements had to reduce throttle to idle and use speed brakes to keep from over-running the formation. No.3 in trail noticed that Lt Clements nozzles were wide open. The EGT of Lt Clements aircraft with throttle at idle was 375 degrees. Lt Clements flew on Lead’s wing to a low key position for a landing from an SFO pattern. At low key Lt Clements noted his RPM was 100%, EGT 375 and oil pressure 40 PSI. The aircraft was configured with gear down, take off flaps down, speed brakes in, throttle in idle, airspeed 240 KIAS. When manipulating the throttle from idle to Military there was little thrust change. Lt Clements turned a wide base leg and airspeed increased to 260 KIAS during the descending turn. He crossed the overrun at about 210 KIAS and touched down at approximately 200 KIAS. A good touchdown was made 500’ from the approach end and center of Rnwy 21. At 170 KIAS the drag chute was deployed, blossomed, and then failed. At 2,200’ remaining the right main tire blew. The pilot noted 150 knots as he went by the 2,000’ remaining marker. He attempted to steer to the center of the barrier but departed the right side of the runway approximately 500’ short and 33’ right of the barrier. At some point the main and nose gear failed. The F-104 continued 1,290’ beyond the end of the runway and came to rest 90 degrees to the runway heading. Fuel on board was 5,500 lbs. The pilot evacuated the aircraft immediately when it came to rest. He was not injured. The engine was still running and stop cocking the throttle did not cut the engine. After the main fuel cut-off switch was deactivated the engine windmilled down. The International F-104 Society owns a copy of the official accident report. |
| 13 March 1961 | F-104A | 56-859 | 157FIS | SC ANG | written off | pilot ok |
| It crashed 4 miles West of Swansea, South Carolina, 9 miles NW of North Field Apt. It toke off from home base Congaree AB and pilot Lt. Michael Martin Miller was ok although injured. The aircraft departed Congaree AB on a scramble mission and climbed to 35000 feet. After appr 15 minutes (0.9 Mach) the pilot was asked to move to 37000 feet. When he advanced the throttle to military setting he experienced slight deceleration. He noticed the RPM drop to 92 % then fluctuating between 92 and 96% accompanied by fluctuation of the exhaust nozzle and fuel flow. The pilot decided to break off the interception and headed back to for an emergency landing. Since he encountered severe problems handling the power of the aircraft he decided to land at North Field Apt at 12 N Miles. Very shortly after the engine flamed out at appr 83% RPM. A number of restarts (incl usage of RAT) failed and the pilot ejected at about 800-900 feet above the ground. Aircraft crashed and exploded in an uninhabited wooded area. Pilot was safe. The International F-104 Society owns a copy of the official accident report. Beneath a photo showing 56-859 at the Congaree AB flightline. It was in use with this unit from February 1960 till its loss. |
| 17 March 1961 | F-104A | 56-819 | 151FIS | Tenn ANG | written off | pilot ok |
| This Starfighter crashed 1.5 miles NNE from Rockford, 3.5 miles from home base McGhee-Tyson Apt, Tennessee. Pilot Major Robert Andrew Bennett was ok. He departed from McGhee on a functional check flight following an engine change. Immediately after takeoff, the gear control handle would not come out of the down position. The pilot limited the speed to try to get the gear up manually which succeeded. To assure that everything was ok he repeated gear down and up with the gear handle. As the gear retracted again the pilot experienced a loud thump, followed by a rise in EGT and a loss of RPM. The sound was not from the closing doors. The engine did not react anymore on the throttle and the pilot decided to eject when he noted the EGT at 950 degrees. His flight took 1 minute and 14 seconds from start to ejection. The pilot sustained no injuries, the aircraft was destroyed by impact and fire. The International F-104 Society owns a copy of the official accident report. |
| 29 March 1961 | F-104F | BB+375 | WS10 | GAF | written off | pilots ok |
| 7 April 1961 | F-104A | 56-757/757 | ChinaLake | US NAVY | written off | pilot killed |
| 9 April 1961 | F-104A | 56-781 | 197FIS | Ariz ANG | written off | pilot killed |
| This F-104A crashed 7 NM WSW of Phoenix Apt, Arizona on a radar interception mission on a T-33, as leader of a 2 ship formation. Pilot Maj Erich Julius Hettlinger was sadly killed while ejecting with his ejection seat. After pilot Hettlinger experienced radio difficulty the mission failed, both lost visual contact with each other, and both returned back to the airbase separately. While flying an approved penetrating CGI on return the pilot experienced malfunctioning speed brake control. One minute later he experienced having only 80% RPM. He was at 3500 feet and descending fast. Before ejecting he was advised to assure he was above unpopulated area. Then he declared a low-oil failure. Soon after the aircraft was seen crashing into a dry river bed without noticing a chute. The pilot ejected sadly unsuccessfully. The seat was found apart from the impacted aircraft. The IFS owns a copy of the official accident report. |
| 5 May 1961 | F-104A | 56-855 | 151FIS | Tenn ANG | written off | pilot killed |
| This F-104A crashed 3 miles NE Alcoa, Knoxville Tennessee, near McGhee Tyson AB. Pilot Capt. Luciano Guida (transition pilot from the Italian Air Force for the AFFTC Edwards AFB) was sadly killed in this accident. It all happened on his 12th flight in his F-104 transition program. Major R.B. Weinard was the leader of the twin flight. During the formation take off roll, Capt Guida did not get een afterburner light and he was informed by the mobile control but sadly did not acknowledge this (perhaps due to radio problems). He continued the takeoff and left the runway and crossed the overrun in a nose high attitude with the tail dragging. He maintained the attitude for 450’ beyond the overrun where he bounced briefly into the air for 170’ and then contacted the ground hard in a porpoise with all three gear for 360. He then bounced into the air again for 150’ and then his right wing dragged the ground for 120’ as he passed the ILS antennae. He again bounced into the air for another 300’ hitting the top of the 5’airport boundary fence which is 1800’from the end of the runway and continuing another 150’into an adjoining field. He lost the ventral fin and engine blow out panel and the ILS antennae. It went airborne again for 800’ clearing a deep ravine and then landing tail first.. At this point the aircraft began disintegrating. The canopy was found 200’ beyond the ravine so it would appear the pilot ejected between the ravine and the canopy. Aircraft was disintegrated and burned. Pilot did not have a change and was found near the seat in which he had ejected. It was a very tragic accident. Note: Capt Luciano Guida was undergoing type conversion with the Tennessee ANG and was selected for the Joint Test Force. It was his last flight at Knoxville, Tennessee. His place was taken by Capt Bonazzi.The IFS owns a copy of the official accident report |
| 5 May 1961 | F-104C | 56-885 | 476TFS | USAF | written off | pilot ok |
| 5 May 1961 | F-104B | 4102 | 8TFS | RoCAF | written off | pilots killed |
| (USAF serial 57-1300) This F-104B crashed in Taiwan sadly killing both pilots, SqCmdr Lt Col Yan Zhong-Hua (37) and Capt (Postumus Major) Yu Hong-Xun (31). After an interception training mission, during the approach at homebase CCK the aircraft entered a roll, probably caused by a "split flap condition" (asymmetric flaps) and crashed near the Northern runway. Yan was one of the first group of 104 instructors in Taiwan and commander of 8 TFS. The aircraft, operated by the 3rd Air Group, 8 TFS, was delivered almost 1 year ago. Beneath a photo taken in 1960 showing this F-104B 4102 when it just had been delivered. |
| 13 May 1961 | F-104C | 56-884 | 476TFS | USAF | written off | pilot killed |
| 22 May 1961 | F-104D | 57-1329 | 479TFW | USAF | incident | pilot ok |
| This Starfighter encountered an accident on Tinker AFB, Ohio. The only pilot, Capt Robert Gerald Ashcraft was ok. He departed George AFB with 4 external tanks (he was instructor pilot) for a VFR mission to Tinker AFB. Upon making a radar approach to Tinker the pilot was sent around due to an emergency in progress. He remained clear of the traffic pattern until the tower stated that the emergency was terminated. The cross wind for landing was challenging especially since the F-104 had become light (low on fuel). To counteract the cross wind he flew down final at 170kts with left wing low and right rudder in. The touchdown was on the left wheel first, then the right wheel. Soon after the right main tire began leaving a heavy black skid mark. The right tire blew out shortly thereafter and the aircraft began to veer to the right. The right turn was stopped and a very gradual left turn started, but not enough to prevent the right main gear from going into the mud on the right side of the runway. Approximately as the left turn began, the pylon tanks were jettisoned from the aircraft. The pilot stop cocked the throttle when the right main gear went off the runway. The 104 continued for a short distance until the right main wheel struck a concrete abutment. At this point the right main gear sheared from the aircraft. The 104 continued on, crossing over the taxy way where the left main and nose gear sheared. It slid to a stop and the pilot could evacuate the aircraft safely. The aircraft was soon repaired. The IFS owns a copy of the official USAF accident report. |
| 25 May 1961 | F-104D | 57-1330 | 435TFS | USAF | incident | pilots ok |
| This F-104D suffered a landing accident at Wright-Patterson AFB, Ohio due to nose-wheel shimmy. Damage was minimal and the crew were safe. Pilots were LtCol Harold E. Collins (Pilot AFSC/ASD Fighter Ops Div at Wright-Patterson) and Capt Kenneth D. Ohman (Instructor Pilot 479TFW/435TFS). They were both on a TAC directed mission to flight test the refueling probe with the KC-135 probe-drogue adapter system. The aircraft was on temporary loan to Fighter Ops Div, Directorate of Flight Test, Wright-Patterson AFB. This day at 1215 hours, the aircraft participated in these tests with LtCol Collins in the front seat and Capt Ohman in the rear. The test portion of the mission was completed in routine fashion, and there was no nose-wheel shimmy on take-off. During landing with approximately 3,000 lbs of fuel remaining, touchdown was made at 155 KIAS at Wright-Patterson, the nose wheel was lowered and nose wheel steering engaged. Severe nose-wheel shimmy developed and nose wheel steering was disengaged. The nose wheel continued to shimmy. To correct shimmy the nose was raised and held off the runway as long as possible. When the nose wheel again contacted the runway the drag chute was deployed. Severe nose wheel shimmy continued with or without nose-wheel steering engaged. Nose wheel steering then failed completely and the aircraft was turned off the runway by using differential braking. It came to rest safely, there was no injury to the crew. Downlocks were inserted, the aircraft was shutdown, and towed to the parking area. Duration of flight has been 2 hours 5 minutes. The IFS owns a copy of the official accident report. |
| 25 May 1961 | F-104A | 56-853 | 157FIS | SC ANG | written off | pilot killed |
| 15 June 1961 | F-104C | 56-897 | 476TFS | USAF | written off | pilot ok |
| While on deployment in Spain this Starfighter crashed 2 NM East of El Coronil, 6 NM South of Moron AB. Pilot Lt. Larry Moench Davis ejected and was ok. He flew a practice scramble intercept mission with Capt. Huffman as lead. After a normal takeoff, as Lt Davis moved his throttle out of afterburner into military position, he felt and heard a chug or thump accompanied by a vibration and a noticeable loss of thrust. His nozzle was full open and oil pressure was around 20psi. Assuming a nozzle failure he pushed the throttle into afterburner trying to light the afterburner. This was unsuccessful. Capt Huffman informed him to pull the emergency nozzle closure handle. This went fine and RPM was 70%. However he did not experience increase of thrust and RPM was limited to 70%. The 104 was now very slow, low and descending and stick shaker was operating. He was advised to eject and this went fine. The aircraft crashed into a hillside and exploded, scattering wreckage for about a quarter of a mile in the line of the flight. Lt Davis landed about 300 yards from the aircraft and was unhurt. He was picked up by a helicopter and returned to Moron AB. The IFS owns a copy of the official USAF accident report. |
| 16 June 1961 | F-104C | 56-932 | 436TFS | USAF | incident | pilot ok |
| This Starfighter encountered an accident after takeoff from George AFB but could be repaired afterwards. Pilot Lt. William Thornton Smith was ok. It departed George with another F-104C to fly to the Cuddeback shooting range on a practice mission for an aerial demonstration which was to be conducted as part of the Falcon 61 project. Upon arrival, appr 15 miles W of the range, both aircraft assumed appr 15 seconds spacing and started a shallow dive towards the range. They had to pass over the range supersonic and pull up to intercept a T-33. During the dive the pilot selected full afterburner and crossed the special weapons target at 1350 feet with 650kts. As the lead pilot began to pull up he experienced what he interpreted to be a severe compressor stall. He immediately performed the stall clearing procedure and obtained to restart which was successful. While climbing to 20000 feet he noted that both leading edge flaps were missing.. At 20000 feet he successfully extended the trailing edge flaps to the take-off position. While slowing to 220kts he encountered severe buffeting and declared an emergency, heading for Edwards AFB. The wingman told him that both main landing gear were extended, doors were missing and the nose gear was retracted. The leader then noted that the gear handle was “up”. However both main gear green lights were on, signifying that gear to be up and locked. He placed the handle to the down position and the nose gear seemed to extend normally, indicating down and locked. No fluid was noted streaming from the aircraft so the pilot made a successful straight-in landing at 240kts including a good working chute. The IFS owns a copy of the official USAF accident report which is sadly not clarifying the exact cause. |
| 26 June 1961 | F-104C | 56-923 | 436TFS | USAF | written off | pilot killed |
| 26 June 1961 | F-104C | 57-917 | 436TFS | USAF | written off | pilot ok |
| 2 August 1961 | F-104C | 56-893 | 476TFS | USAF | written off | pilot killed |
| This F-104C crashed 44 NM SE of Moron, 3 NM E of town Jubrique in Spain during a deployment. Pilot 1st Lt Johny Lee King was sadly killed. That afternoon 4 aircraft flew a 2 to 2 intercept and simulated air combat training mission. Pilots were Lt Tamm, Lt Plummer, Major Loeffler and Lt King. Lt Tamm and Lt King were the flight leaders. During this mission on one moment the other three aircraft lost contact with Lt King. It was just after they had been in a steep dive attitude. Then Major Loeffler noted smoke behind and below him on the ground and saw that this was the aircraft of Lt Kind who had crashed. The cause of the accident is unknown but could well have been caused by loss of control of the aircraft due to disorientation or technical failures. It crashed approximately 18 minutes after takeoff. The IFS owns a copy of the official USAF accident report. |
| 5 August 1961 | F-104B | 57-1306 | 151FIS | Tenn ANG | incident | pilots ok |
| This F-104B suffered a landing accident at McGhee-Tyson Airport, Tennessee following an AB nozzle failure in flight. The aircraft was damaged after leaving the runway with left main and nose wheel gear failure. Both pilots were uninjured. The crew was IP Captain Robert W. Cantrell with pilot 1Lt Taft L. Davis both of 140th ADW, 134th FG, 151st FIS, Tennessee ANG. This flight was a scheduled morning acrobatic flight in the local area, but just after take-off and AB climb to 35,000 ft two minor aircraft discrepancies occurred causing the pilots to abandon the acro mission. When the throttle was withdrawn from afterburner range the AB nozzles failed to close. Capt. Cantrell tried an immediate AB relight with no success. Unable to maintain altitude he started a turn back to base and notified them of the emergency. Nozzle over-ride had no effect from either the front or rear cockpit. The crew then went through nozzle failure procedure. Tip tanks were jettisoned over the mountains. Throttle was left in AB range to burn off fuel along with t/o flaps. A straight-in approach to Rnwy 04L was made from 11,000 ft. The pilot extended the speed brakes and did several S turns to lose altitude. Repeated attempts to relight the AB failed. At 2,000 ft the throttle was retarded, slowing to 240K, and the gear was lowered. The engine was shut down while still airborne and touchdown was at approx 200 knots and 2,500 ft down the runway. Just after landing the nose was lowered and drag chute deployed. The drag chute came out, blossomed, than immediately collapsed. During heavy braking the left main tire blew out with just 1,900 ft of runway remaining. The aircraft started a slow drift to the left and the pilot could not maintain directional control with braking action. The F-104 departed the runway at the junction of the taxi strip and the end of the runway at about 50 knots. The left gear struck an approach light and sheared off. Continuing into a left turn, the side load caused the nose wheel to shear off. The aircraft came to rest in an area of runway construction resting on its left wing, nose gear doors and right gear. It had stopped 800 ft past the end of the runway and 90 degrees off the runway heading. The pilots escaped without injury. Duration of flight was just 7 minutes. The IFS owns a copy of the official USAF accident report. Beneath a photo showing this F-104B with markings of this 151FiS, taken around or in 1961. |
| 11 August 1961 | F-104C | 56-899 | 436TFS | USAF | incident | pilot ok |
| This F-104C was substantially damaged after an emergency, hard landing which failed all three landing gear on Cuddeback Lake, California. The pilot was not injured. The emergency was initiated by a nozzle failure. The pilot was 1Lt Stephen M. Korcheck with 479-TFW, 436-TFS. Mishap occurred while flying a 3-ship bombing and gunnery mission at the Cuddeback Range. Two dry runs were made at Leach Lake, then four bombing runs done at Cuddeback. Two additional runs were then planned to burn off fuel. On the second of these passes Lt. Korcheck pulled off and experienced loss of thrust and an oil level warning light. His nozzles were open to 7 and oil pressure 20 psi. He pulled the emergency nozzle closure handle and the nozzles closed properly. Lt Korcheck climbed and turned to southwest and announced that he would land at Cuddeback Lake. His power was apparently good. The approach was normal until over the lake bed when depth perception was impaired by loss of vertical reference. The aircraft touched down hard which snapped the main gears on initial impact. Lt Korcheck felt that the landing was good and didn’t realize that he was riding on the MN-1A Dispenser. He pulled the drag chute but it did not deploy as the door was already damaged and the aircraft skipped and slid on the tip tanks and dispenser until the nose gear collapsed striking the canopy. The F-104 veered sharply to the right, breaking the fuselage just forward of the intake ducts and slid to a stop 160 degrees from the landing heading. Lt Korcheck opened the canopy, pulled the spur cutter handle and evacuated without injury. Duration of flight was 1 hour 9 minutes. The aircraft was extensively damaged but could be repaired again. The IFS owns a copy of the official USAF accident report. Beneath a photo of the aircraft taken in 1962, a year after the accident. |
| 28 August 1961 | F-104C | 56-913 | 434TFS | USAF | written off | pilot killed |
| 31 August 1961 | F-104B | 57-1307 | 151FIS | Tenn ANG | incident | pilots ok |
| This F-104B suffered a landing accident and was damaged at Campbell Army Air Field (Fort Campbell), Kentucky. Both pilots escaped without injury. The crew was IP Captain Alvin R. Ruthstein and student pilot 1Lt Errol L. Johnstad, both of ANG/ADC, 134-FG, 151-FIS, Tennessee ANG. The purpose of this flight was for Lt Johnstad to get his final dual ride prior to solo checkout. Take off from Berry Field (now Nashville IAP), Tennessee was normal and a touch and go landing was made on Rnwy 31 at Berry Field. Airspeed was at 175 knots on the rollout but as the aircraft crossed the runway threshold about 30 or 40 feet in the air both pilots stated that the rate of sink became excessive. Both pilots pulled back on the stick and throttled to Military but the aircraft struck the runway hard and bounced. Capt Ruthstein lit the afterburner and took the aircraft up and around. From this time forward Capt Ruthstein did all of the flying from the rear cockpit. Mobile control informed the crew that the right main landing gear had been damaged. Another F-104 was scrambled to check them over. This F-104 joined up and told the crew that the right main gear was broken off and dangling by the oleo strut. Capt Ruthstein decided to land at Campbell AAF (Fort Campbell, Kentucky) and requested the runway be foamed. When told this would take 25 minutes he decided not to wait and set up for landing. He burned fuel down to 600 lbs first. The F-104 touched down very light on the left main on Rnwy 22 at Campbell AAF, and the nose was lowered. The drag chute was deployed successfully and the right tip tank contacted the runway. Directional control was maintained with nose wheel steering for over 1,000 ft. As nose gear steering lost effectiveness the aircraft gradually turned right and departed the runway at the 3,200 foot mark. It continued another 400 ft ending up 90 degrees to the runway heading. The F-104 crossed a small ditch and collapsed the nose and left main gears. The pilots evacuated safely and there was no fire. Duration of flight was 6 minutes. The aircraft was repaired again. The IFS owns a copy of the official USAF accident report. |
| 6 September 1961 | F-104F | BB+378 | WS10 | GAF | written off | pilots ok |
| This two-seater crashed after a total navigation-equipment-failure near Neckarmuhlbach and Siegelsbach (Near Mosbach/baden). This navigation problem resulted in running out of fuel and subsequent flame ouy of the engine. Olt Erwin Willing and Olt Hermann Hammerstein ejected and were safe. Beneath a small photo showing the aircraft around 1960. |
| 7 September 1961 | QF-104A | 56-746 | 3205DS | USAF | incident | pilot ok |
| 7 September 1961 | F-104A | 56-811 | 151FIS | Tenn ANG | incident | pilot ok |
| 29 October 1961 | F-104C | 57-926 | 435TFS | USAF | incident | pilot ok |
| This F-104C suffered a ground accident preparing for t/o roll at Ramstein AB, Germany when on deployment. The right main landing gear had apparently failed. There was no injury.Pilot was 1Lt George F. Tommasi with 435-TFS, 479-TFW. He was commencing take off on runway 27 at Ramstein AB, Germany for a 2-ship practice air defense mission. When full Military power was attained prior to take off the pilot heard a loud BANG and felt the aircraft settle onto the right wing. The pilot shut down because the aircraft was resting on the right pylon tank. The aircraft was removed from the runway without further incident and could be repaired. The IFS owns a copy of the official USAF accident report. |
| 14 November 1961 | F-104D | 57-1326 | 476TFS | USAF | incident | pilots ok |
| On this day this F-104D departed the runway upon landing at George AFB, California. The crew was safe. The aircraft was piloted by 1Lt David H. Groark (student) and Captain Sam C. Henley (IP) both with 476-TFS, 479-TFW. This accident occurred following a normal, night checkout mission for Lt. Groark in the front seat (approx 1900 local time). Approach and letdown to Runway 16 at George was normal although one go around had been made when Lt Groark had lost too much altitude and airspeed on the first attempt to land. Downwind and base legs were adequate and the final approach looked good to mobile control, tower and both pilots until a point about 2,000’ from the end of the runway. At this point the IP (Capt Henley) told Lt Groark to add power and grabbed the stick himself. Immediately thereafter the aircraft struck the overrun approximately 780 ft short of the runway threshold. The F-104 bounced about 4 ft in the air and again touched down on the overrun when it then bounced up to and on the runway. The IP gained control and maneuvered the aircraft onto the runway with rudder. The IP attempted to maintain control with left brake when on the runway and the drag chute was deployed. The F-104 veered off the runway to the right and could not be controlled so the IP stopcocked the throttles. The aircraft departed the runway to the right 2,000 ft past the landing end, went down a slight decline and up a slight rise of sand where it came to a stop about 360 ft off the side of the runway at an angle of 60 degrees off runway heading. The 2 pilots abandoned the aircraft without incident. Duration of flight was 1 hr, 35 min. The IFS owns a copy of the official USAF accident report. |
| 21 November 1961 | F-104A | 56-756 | AFSC | USAF | incident | pilot ok |
| 25 November 1961 | CF-104 | 12712 | Canadair | CAF | written off | pilot ok |
| 27 November 1961 | JF-104A | 55-2966 | AFSC | USAF | incident | pilot ok |
| 9 December 1961 | F-104A | 56-841 | 157FIS | SC ANG | written off | pilot ok |
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