| 29 January 1959 | F-104C | 56-907 | 434TFS | USAF | written off | pilot ok |
| 9 February 1959 | F-104C | 56-921 | 434TFS | USAF | incident | pilot ok |
| It encountered an accident at George this day but could be repaired soon after. The pilot Lt Col Charles W. Boedeker (434 TFS) was returning from a local night flight when he touched short of the overrun about 1.000 feet short of the runway. The aircraft skidded over the overrun, past the approach end barrier and came to an abrupt stop about 5.300 feet down the runway when the main landing gear collapsed completely. Pilot Lt Col Charles W. Boedeker was ok and left the aircraft on his own. Aircraft could not be repaired at the base and had to be sent to Lockheed. The IFS owns a copy of the official accident report. |
| 13 February 1959 | F-104A | 56-783 | 538FiS | USAF | written off | pilot ok |
| 28 February 1959 | F-104C | 56-892 | 476TFS | USAF | incident | pilot ok |
| This Starfighter suffered a right main gear tire failure on takeoff at George AFB, California. The runway barrier cable failed and the aircraft departed the overrun, collapsing all three gear, and was heavily damaged. The pilot , Colonel Darrell S. Cramer, 479-TFW, 476-TFS , suffered only minor injuries. This was a planned 4-ship practice mission for a long-range air refueling mission simulating flight to Hawaii. Four external tanks were carried (two tips, two pylons). One of the four aircraft was cancelled due to malfunctioning APC system. Flying as flight leader 56-892 started take-off roll with No.2 and No.3 following in 8 second intervals. Approx. 5,000 ft down the runway and 170 knots, Colonel Cramer felt vibration which he at first believed to be nose wheel shimmy. The vibration increased so rapidly he realized he had a right main gear tire failure. He was forced to abort t/o, jettisoning his stores, stop cocking the throttle and deploying the drag chute. Vibration at this time was so severe the pilot was unable to read his instruments. The external tanks struck the runway and continued on the runway for a short period then went off either side at 15 to 25 degree angles. Fuel in the tanks had ignited. The F-104 straightened out and then veered left engaging the barrier left of center. The barrier arresting cable failed allowing the aircraft to continue off the end of the runway where all three gear collapsed. The aircraft came to rest 1,500 ft past the overrun end cocked to the right. The pilot egressed with only minor bruises. The No.2 and No. 3 pilots, not realizing soon enough that there was a problem, made successful takeoffs flying through the smoke, dust and debris from the lead airplane. There was no damage to these two airplanes. The IFS owns a copy of the official accident report. |
| 19 March 1959 | F-104C | 56-900 | 476TFS | USAF | written off | pilot ok |
| 6 April 1959 | F-104A | 56-765 | 83FiS | USAF | written off | pilot ok |
| 16 April 1959 | YF-104A | 55-2971 | ARDC | USAF | incident | pilot ok |
| In 1959 this YF-104A damaged its undercarriage when it run off the runway during a barrier test program. By that time the aircraft was named “Slosher nr II”. The pilot had ejected the canopy but stayed inside the aircraft. |
| 20 April 1959 | F-104A | 56-812 | 83FiS | USAF | written off | pilot killed |
| 28 April 1959 | F-104A | 56-757 | AFSC | USAF | incident | pilot ok |
| This Starfighter had an incident at Holloman AFB, NM this day. On routine GAR-8 Sidewinder test mission as aircraft took off and retracted gear, the pilot noticed a fire warning light. Pilot zoomed to bailout altitude but fire light went out. Tower radioed no evidence of fire on the airplane. Pilot recovered safely back to Holloman. No injuries and no damage to aircraft. Pilot was Major Thomas McElmurry. Attached to ARDC. The IFS owns a copy of the official accident report. |
| 24 May 1959 | F-104A | 56-796 | 83FiS | USAF | incident | pilot ok |
| 15 June 1959 | YF-104A | 55-2956 | ChinaLake | USNavy | written off | pilot ok |
| This aircraft, belonging to the US Navy China Lake AIM9 test team, encountered a severe accident this day. Pilot CMDR Herkimer “Herk” Kamp gladly survived the accident. It was lost during takeoff at NAF when it encountered an engine failure and by trying to stop it ran off the runway where the undercarriage collapsed. It was declared written off although at first sight the aircraft looked to be repairable. However the structural damage to the bottom of the aircraft and internally to the airframe itself was significant. It was replaced by 56-740 soon after. It is not clear what happened to the remains of this “956” but at least it was scrapped.. Surprisingly both USAF and USNavy do not own any accident report regarding this accident. Beneath photos of the aircraft before and after the crashdate. (Thanks to Larry Ruybal and Gary Verver) |
| 17 June 1959 | F-104C | 56-901 | 434TFS | USAF | incident | pilot ok |
| It had an accident this day at Edwards AFB while based at George. Very likely the pilot (Roth) was ok. Chris Baird made a short summary: In the evening at 22:23 local time, this Starfighter suffered engine malfunction and loss of thrust while refueling. It reached Edwards Air Force base for an emergency landing.It managed to reach the runway but due to the high speed it overrun collapsing its complete undercarriage. The aircraft slid for about 6,500 ft and was substantially damaged. The pilot (2Lt Daryl E. Roth, 479-TFW, 434-TFS.) was gladly ok. This mishap occurred in flight of three F-104Cs from George AFB on night-refueling mission with KB-50Js in clear weather conditions. After about 75 minutes after takeoff the refueling began. 2Lt Roth, flying as No.2, attempted four times to hook up to the KB-50J which was maintaining 208-2110 knots. He was unable to maintain position. Several more hook-ups were attempted but he could not obtain closure speed. A hook-up was finally made but then 2Lt Roth experienced a large loss of thrust. Instruments showed EGT 600 degrees, fuel flow steady, nozzle position 2.5, and RPM stabilized at 70%. When the throttle was retarded to idle then advanced rapidly to military there was no increase in RPM or thrust. This was done 3 times with no affect at which time airstart was actuated and power was regained. Lead aircraft instructed Roth to return to George. When 56-901 made a right turn towards George another loss of thrust was experienced. Clearing procedure was done again and power was regained again. The pilot climbed to 35,000 ft then made AB climb to 40,000. But a descent of 1,200 to 1,600 ft per minute was required to maintain 275 knots. A decision was made to land at Edwards AFB 15,000 ft runway on the lakebed. During descent 2Lt Roth passing through 27,000 ft noticed that he had 92% RPM indicated as compared to 83% the lead pilot reported he was carrying to maintain wing position. A high key point was set over Edwards AFB at about 20,000 ft and power set to 85%. The precautionary pattern was flown with an apparent normal rate of descent. Flare was made at about 200 knots and touchdown at 190 knots. Touchdown occurred on the concrete overrun 750 short of the threshold lights. Immediately on touchdown the main landing gear struts were forced through the air inlet ducts allowing the main gear to spread out and up so that the wings rested on the wheels. The nose gear was sheared off at touchdown and the aircraft slid on its belly for 6,500 ft burning on its underside throughout the slide. The pilot evacuated safely and was uninjured. The F-104 was significantly damaged but could be repaired. The IFS owns a copy of the official accident report. |
| 23 June 1959 | F-104A | 56-742 | G.E. | USAF | written off | pilot killed |
| 30 June 1959 | F-104A | 56-768 | ARDC | USAF | written off | pilot ok |
| This Starfighter was written off after an accident during takeoff from Edwards AFB, Calif. Pilot Capt. Norvin “Bud” C.Evans made a successful ejection after a broken oil-line caused a fire. This F-104A flew as an AFFTC support aircraft at Edwards AFB. On this date it was flying a chase support mission (X-2) with an F-11F Tiger flown by RCAF Lieutenant Jack Woodman. The F-104 made a normal AB take-off seven seconds behind the F-11F from Runway 4 at Edwards AFB. After becoming airborne, strong fumes were noted in the cockpit. Instrument readings appeared normal however and the fumes dissipated. A max afterburner climb was made to approximately 45,000ʼ and the flight continued in the supersonic corridor in the vicinity of Cuddeback and Harper Lakes descending to 35,000ʼ and performing S-turns in the corridor. Coming out of AB to .9 Mach as the flight turned out of the west end of the supersonic corridor, engine roughness and noise caused the pilot to check oil pressure, which was passing through 30 PSI and dropping steadily. The F-104A and F-11F then commenced a return to base due to the malfunction. On descending approach to Edwards the F-104 continued a steady drop in oil pressure with intermittent engine vibrations. Oil pressure dropped to zero about 30 miles west of the town of Rosemond. The pilot increased throttle to 96% and attempted a straight-in approach to Runway 4 at Edwards AFB. He turned long final at 9,000ʼ and 400 knots with rapidly decreasing airspeed and heavy engine vibration (the time was 1821 hours). As he actuated the speed brakes the engine began grinding loudly and vibrating heavily. The radio failed as he was transmitting his difficulties. The nozzles began oscillating between full open and full close. The throttle was closed. Airspeed bled off to 250 knots passing 7,000ʼ in a steep descent. The aircraft was vibrating heavily and yawing left and right. Smoke began to pour into the cockpit as well as the smell of hot metal. The pilot hooked up his zero lanyard, pulled back on the stick and ejected at appr 2,500ʼ as the aircraft pitched up. The seat remained in close proximity to the pilot so that only the lap belt release was actuated even though the zero lanyard was attached. Pilot had to manually actuate the D-ring and his parachute deployed normally at 1,000ʼ. The pilot landed safely. The F-104 crashed into the ground and exploded. Total duration of flight was 23 minutes. The crash occurred 4 miles from the approach end of Runway 4 at Edwards AFB. The investigation revealed the oil pressure loss was caused by a rupture in an expandable oil line. The loss of cooling oil melted the compressor bearings, which caused the compressor blades, rotating at 18,000 rpm, to shift, impacting the fixed stator blades and destroying the engine. Regarding the problems with the ejection seat. an examination showed that the cable, which was attached to the firing initiator, was wound in three loops and encased under a plate that was bolted to the seat front. The last time the seat was inspected, the last loop had gotten wedged between the seat and the plate when the cover plate was bolted to the seat. The investigators estimated that to stretch the inside strands of that trapped loop one-sixteenth of an inch, just enough to fire the seat ejection cartridge, The pilot had to have pulled hard enough to create a force of 450 pounds.. The IFS owns a copy of the official accident report. |
| 7 July 1959 | F-104A | 56-815 | 83FiS | USAF | written off | pilot ok |
| 16 July 1959 | F-104C | 56-905 | 434TFS | USAF | incident | pilot ok |
| At 10:11 local time, this F-104C suffered a right main tire failure on takeoff from George AFB, California. The pilot aborted the takeoff and engaged the barrier dead center. The aircraft decelerated and came to rest off the right side of the overrun in the dirt. There was no fire. The pilot, 1Lt Morris B. Larson of 479-TFW, 434-TFS was unhurt. Taking-off in formation as No. 2/Wing, Lt Larson felt the right main gear tire blow at 4,200 ft down the runway and appr 150 knots. He started to veer towards Lead and corrected with left brake and reduction of power to avoid collision. The pilot then aborted t/o, reducing throttle and engaging nose wheel steering and deploying drag chute. The pilot was able to keep the F-104 centered and radioed that he was taking the barrier. Aimed at the center of the barrier he moved throttle to OFF. A successful barrier engagement was made and the aircraft decelerated, then veered right into the dirt just off the hard overrun surface. The pilot engaged the fuel shut off switch, opened the canopy and evacuated without injury. The IFS owns a copy of the official accident report. |
| 20 July 1959 | F-104A | 56-836 | 538FiS | USAF | incident | pilot ok |
| Together with another F-104A he took off from Larson at appr 11:50 PST on a local IFR tactical action flight. After completing the intercept portion of the mission he returned back to Larson. Appr 3 miles out on final he was advised to break right out of traffic due to 2 Marine A4D jets ahead of him on final approach. He immediately broke out and initiated a go around. he raised the gear and flaps. When he got clearance for runway 21 the pilot, Capt Wesley Earl Brown, called gear down and preasure up on base leg. The miscommunications (possibly radio interference) with the tower resulted in the aircraft touching down with gear up and locked. The aircraft slid to a stop and happily no fire followed. The pilot evacuated the aircraft immediately with apparent injury. The aircraft was withdrawn from operational usage, went to Lockheed for instructional use, and was modified to QF-104A by Lockheed by September 28, 1962. The IFS owns a copy of the official accident report. Photos thanks to Ian Wallace. |
| 11 August 1959 | F-104A | 56-825 | 83FiS | USAF | written off | pilot ok |
| 19 October 1959 | F-104B | 56-3724 | 337FiS | USAF | written off | pilots killed |
| This day this F-104B crashed near Templeton, Massachusetts while performing an instrument proficiency check flight. Both pilots ejected but did not survive. Instructor pilot was Captain James T. Akeley and co-pilot was 1Lt Peter A. MacBurnie both of 337-FIS. About 20 minutes into the flight the crew requested a practice UHF/DF problem from Westover tower while on a 060 degree heading at 20,000’ but the crew did not re-contact the tower on the proper channel to perform the problem. 15 minutes later the crew contacted Boston Air Defense Sector (SAGE) and requested recovery while flying 030 degrees and 30,000’. They were told to make a starboard turn to 230 degrees and descend to 10,000’. The mishap F-104 acknowledged passing through 15,000’ and traffic. A corrective turn was then ordered but the F-104B did not respond. About the time that SAGE was to hand over to terminal approach control all SIF and radar contact was lost with the F-104. The time was 1407Z. Duration of the flight had been 50 minutes. The Massachusetts State Police later contacted Base Operations at Westover AFB informing them of an aircraft crash near Templeton, Massachusetts. An SA-16 pilot dispatched to the location reported the debris and fire at 1720Z. At 1825Z a report was received that two bodies had been found at the crash site. At 1842Z the wreck was confirmed to be an F-104. The cause of the fatalities was ejection at too low an altitude for survival. Cause of the accident became undetermined. The IFS owns a copy of the official accident report. |
| 28 October 1959 | F-104C | 56-915 | 436TFS | USAF | written off | pilot ok |
| 2 November 1959 | YF-104A | 55-2964 | ARDC | USAF | written off | pilot ok |
| 2 November 1959 | F-104A | 56-733 | ARDC | USAF | incident | unknown |
| This aircraft encountered a severe accident this day but could be repaired soon again. It was officially reported on the USAF list but sadly the USAF did not have any accident report available. It looks like no pilot was involved in the accident. |
| 6 November 1959 | F-104A | 56-791 | 83FiS | USAF | incident | pilot ok |
| This aircraft while at McClellan AFB (AMC, SMAMA) undergoing IRAN suffered a landing accident (on Runway 16 at McClellan) resulting in repairable damage. Flight Test pilot Captain Jimmie Pierce received minor injuries. The aircraft had previously been test flown twice by Capt. Pierce with numerous discrepancies discovered on both flights. Capt. Pierce discussed the previous problems with a Lockheed Technical Representative before this third flight. The aircraft was serviced with 5,850 pounds of internal fuel with no external tanks attached. After take-off and accelerating to climb-out speed in a left turn the pilot noted heavy fuel fumes. The pilot immediately switched to 100% oxygen and notified the tower. The tower cleared him for emergency landing and dispatched fire trucks. After rolling out of the initial left turn Capt Pierce climbed to 10,000-11,000 feet to reduce speed and gain altitude for a low key entry to a forced landing pattern. He placed the flaps in t/o position and then lowered the gear shortly after calling “low key” to assure establishing a safe gear condition. As the pilot rolled out on final approach, he noted the airspeed at 260-to-270 knots and determined his touchdown point would be half-way down the runway. Capt. Pierce elected to lower land flaps and extend the dive brakes in order to descend more rapidly until intercepting a more favourable final approach glide. But as he passed through 2,000-3,000 feet he became aware of an increasing rate of sink. He immediately retracted the dive brakes, rotated the nose up, and advanced the throttle to full military. Airspeed at this time was 220 knots. The pilot could not break the rate of descent with full military power and rotation of the aircraft. He did not use afterburner because of the previous fuel fumes. The aircraft hit hard on the tail section and main gear near simultaneously at a distance 72 feet past the beginning of the asphalt overrun. The plane continued approx 900 feet before the nose gear contacted the overrun. 300 feet after contacting the overrun the nose tire blew out. The aircraft continued down the runway, grinding away the nose wheel; 2,700 feet after the nose tire blew, one half of the nose wheel had ground off and the other half fell away from the strut. The plane travelled another 1,000 feet partially grinding off the piston portion of the nose strut, before coming to a stop. The tower had notified Capt Pierce that he was on fire during the landing roll. However, the fire was only the sparking and flash burning of the magnesium being ground off the nose strut. The fire went out before the aircraft stopped. Capt Pierce evacuated the aircraft suffering severe back pains. the pilot hurried back to safe the ejection seat after he had evacuated. Damage to the aircraft turned out to be relatively minor. Damage Report lists the following description of damage: nose gear ground off, nose gear doors DBR, pitot boom damaged and skin on bottom of aft fuselage buckled and torn. Estimated cost of repair: $2,866.00 (350 man hours to repair) The IFS owns a copy of the official accident report. Beneath a photo of this 56-791 released by USAF. |
| 10 November 1959 | F-104B | 57-1295 | 83FiS | USAF | written off | pilots ok |
| 12 November 1959 | F-104C | 56-916 | 476TFS | USAF | written off | pilot ok |
| 13 November 1959 | YF-104A | 55-2965 | ARDC | USAF | incident | pilot ok |
| Crash landed and was repaired later on. At approximately 1120 hours PST this day, this aircraft with pilot Capt George Paul Eremea, was involved in an accident during a dead engine approach and landing at “Bicycle Lake” Camp Irwin, California. The aircraft received major damage. The pilot was gladly uninjured. The aircraft departed Edwards Air Force Base at 1100 hours PST on a local VFR clearance for a test flight due to maintenance performed on the afterburner fuel system (X-3). Fuel on board at take-off was approximately 905 gallons, Fuel on board at the time of the accident was approximately 320 gallons. The weather was high thin broken 14 miles visibility, temperature 66 degrees F. Winds were light and variable. A normal afterburner takeoff and climb in easterly direction to 30000 feet was performed. During the various tests executed on the engine AB system suddenly the fire warning lights started to illuminate when the engine passed 72% RPM. Because of these lights the pilot decided to make a dead engine emergency landing on the dry lake North East of camp Irwin. The throttle was moved to idle cut-off and the fire warning lights went out. A glide towards Bicycle Lake was established at approximately 260knots. A pattern was planned for a 270 degrees approach to runway 04. At the turn onto downwind the altitude was 13000 feet and the ram-air turbine was extended. Evidence of a proper extension was noted by illumination by some lights on the master caution panel. From baseleg turning ontofinal the altitude-attitude seemed a little too low for the baseleg position. The turn was tightened a little to reduce the distance to touchdown. The aircraft was purposely dived toward some low hills (appr. 400 feet high) which were in line with the final approach. At approximately 3700 feet indicated altitude a gradual flare was started. Just short of the lakebed the landing gear handle was placed in the down position and the emergency landing gear lanyard was pulled and held until the aircraft touched down. Approximately 4 seconds time elapsed. During the flare the rate of sink seemed unusually high although the airspeed was 255 knots at the start of the flare. Airframe buffet, possible stick shaker actuation, and some lateral control problems were experienced just prior touchdown. The control stick was intentionally pushed forward slightly to commit the aircraft to touch down and to prevent the tail of the aircraft from dragging. Just after the aircraft touched down the dragchute handle was pulled and at the same time the left wing dropped. The drag chute failed to deploy and the aircraft started to veer slightly to the left. The speed brake was moved to the open position. Heavy right braking was used in an attempt to maintain directional control. In addition to veering to the left, the aircraft began to skid to the right as two banks of loose dirt bordering runway 13-31 were approached. The shoulder harnass was locked and the canopy was fully opened prior to hitting the banks of dirt (approximately 12 inches high and 36 inches wide, separated by approximately 200 feet). When the first bank of dirt was crossed a very large jolt was experienced. A much less severe jolt was experienced as the second bank of dirt was crossed. The aircraft came to rest off the edge of the lakebed, approximately 1000 feet from the second bank of dirt heading 265 degrees after approximately 4700 feet ground distance. Of the 135 degrees turned from touchdown to a complete stop the greatest amount of turn occurred in the last 500 feet of distance traveled. The aircraft skidded approximately 25 degrees as it had stopped. The pilot evacuated the aircraft prior to the arrival of the crash crew. The IFS owns a copy of the official accident report. Beneath some photos showing the damage of the aircraft. (Thanks to Chris Baird) |
| 14 December 1959 | F-104A | 56-895 | 476TFS | USAF | written off | pilot ok |
| It crashed somewhere in Spain while being stationed at Moron. Pilot Raymond L. Krasovich ejected safely. Capt Raymond L Krasovich (flight leader of two) departed from Moron AB on an air-to-air refueling mission. After the gear and flaps were up, the pilot retarded the throttle out of AB. When in flight he retarded the throttle appr. 1/8 of an inch , the pilot heard a muffled explosion followed by a rumble and a corresponding loss of thrust. He informed the wing man that he had an engine failure, jettisoned the tip tanks and started a left turn to Moron. While retarding to idle and then to military power again the rumbling and lack of thrust continued. Reaching 230 KIAS the aircraft was buffeting and descending and the pilot ejected at 800-900 feet above the terrain. The pilot’s chute did not open completely but he landed in an olive tree and survived with only minor injuries. The IFS owns a copy of the official accident report. |
| 15 December 1959 | F-104A | 56-796 | 83FiS | USAF | incident | pilot ok |
| 16 December 1959 | F-104A | 56-795 | 83FiS | USAF | incident | pilot ok |
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